88
Complaints Reported

Complaints by Component

ENGINE AND ENGINE COOLING
16 complaints
CRACKED "Y" PIPE IS LEAKING DIESEL EXHAUST FUMES INTO CAB OF TRUCK. THIS OCCURRED PREVIOUSLY WHEN THE TRUCK WAS UNDER WARRANTY BACK IN 2004 BUT NOW IT IS NOT UNDER WARRANTY NOR IS THERE A RECALL. I HAVE BROUGHT THIS UP TO SEVERAL DEALERS IN THE AREA BUT UNLESS IT IS UNDER WARRANTY THEY WON'T COVER THE REPAIR. HOWEVER, I FEEL IT IS A MAJOR SAFETY HAZARD WHICH I FEEL SHOULD BE ADDRESSED IMMEDIATELY, AS DIESEL FUMES ARE LINKED TO CANCER OR COULD LEAK TO AN ACCIDENT IF SOMEONE IS OVERCOME BY THE FUMES, WHICH COULD LEAD TO A DEATH. PLEASE LOOK INTO THIS HAZARD AND LET ME KNOW IF YOU HAVE ANY QUESTIONS, I WOULD BE HAPPY TO ANSWER. I DO KNOW FROM TALKING TO MECHANICS THAT THIS DOES OCCUR OFTEN IN THESE TRUCKS.
Feb 27, 2014
TL* THE CONTACT OWNS A 2003 FORD F350 DIESEL. THE CONTACT STATED THAT THE VEHICLE COULD NOT BE STARTED IN COLD WEATHER. THE VEHICLE WAS TAKEN TO THE DEALER SEVERAL TIMES FOR THE FAILURE. THE DEALER PERFORMED A DIAGNOSTIC WHICH LOCATED THE FAILURE AT THE EGR EXHAUST SYSTEM VALVE BUT THE DEALER DID NOT REPLACE THE EGR VALVE. THE VEHICLE WAS THEN TAKEN TO A LOCAL MECHANIC FOR A SECOND DIAGNOSTIC WHICH LOCATED THE FAILURE AT THE FUEL INJECTION CONTROL MODULE BOX AND THE GLOW PLUGS MODULE. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS CONTACTED AND DENIED ASSISTANCE WITH THE REPAIRS DUE TO THE AGE OF THE VEHICLE. THE FAILURE MILEAGE WAS 10,000 AND THE CURRENT MILEAGE WAS 111,000. UPDATED 03/05/12*LJ THE ENGINE GLOW PLUG WAS REPLACED. UPDATED 03/08/12
Jan 30, 2012
TL*THE CONTACT OWNS A 2003 FORD F-350. THE CONTACT STATED THAT WHILE DRIVING 45 MPH, A SPARK PLUG FLEW OUT OF THE ENGINE COMPARTMENT AND HIT THE HOOD OF THE VEHICLE. THE VEHICLE WAS TAKEN TO A REPAIR SHOP WHERE A COIL AND THE SPARK PLUG WERE REPLACED. THE FAILURE OCCURRED TWO ADDITIONAL TIMES AFTER. THE VIN WAS UNAVAILABLE. THE FAILURE MILEAGE WAS APPROXIMATELY 98,000 AND THE CURRENT MILEAGE WAS APPROXIMATELY 101,000.
Oct 20, 2010
DT*: THE CONTACT STATED WHILE DRIVING THE VEHICLE STALLED AND LOST POWER. THIS OCCURRED AT VARIOUS SPEEDS, AND IN ALL INCIDENTS THE VEHICLE RESTARTED. THE VEHICLE WAS LATER DRIVEN TO THE DEALER, WHO REPLACED AND REPROGRAMMED THE TURBO-CHARGER. HOWEVER THIS DID NOT REMEDY THE PROBLEM. ON THE MOST RECENT VISIT TO THE DEALER THE TURBO CHARGER WAS REPLACED, BUT THE PROBLEM STILL OCCURRED. UPDATED 05/30/06. *AK
May 09, 2006
CONSUMER REQUEST FOR REIMBURSEMENT FOR ENGINE REPLACEMENT IN THE 2003 FORD F350.*MR THE CONSUMER HAD A MULTITUDE OF PROBLEMS WITH THE VEHICLE LACKING POWER AND BLOWING OUT WHITE SMOKE, AT TIMES THE VEHICLE WOULD HESITATE ON START UP, IT JERKED WHEN THE CONSUMER ATTEMPTED TO ACCELERATE, THERE WAS A RATTLING NOISE WHEN THE CONSUMERS FOOT WAS RELEASED FROM THE ACCELERATOR. THE INTAKE MANIFOLD HAD POPPED LOSE. THE CONSUMER WAS TOLD BECAUSE AN AFTER MARKET CHIP WAS INSTALLED IN THE VEHICLE, THE ENGINE WOULD NOT BE COVERED UNDER WARRANTY. *JB
Aug 30, 2005
+ 11 more complaints for this component
VEHICLE SPEED CONTROL
12 complaints
TL* THE CONTACT OWNS A 2003 FORD F-350. THE CONTACT STATED THAT WHILE DRIVING 65 MPH, HE LOST CONTROL OF THE VEHICLE AS THE VEHICLE INDEPENDENTLY DECELERATED TO A COMPLETE STOP. THE VEHICLE WAS TOWED TO THE DEALER FOR DIAGNOSIS. THE DEALER STATED THAT THE AIR BLOCKERS FAILED AND NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS CONTACTED AND ACKNOWLEDGED THE FAILURE BUT PROVIDED NO ASSISTANCE. THE FAILURE AND THE CURRENT MILEAGE WAS 98,000.
May 23, 2012
TL*THE CONTACT OWNS A 2003 FORD F350. THE CONTACT STATED THAT THE VEHICLE SLOWLY GAINED SPEED DURING ACCELERATION. THE VEHICLE HAS BEEN TO THE DEALER ON SEVERAL OCCASIONS FOR THIS ISSUE AND WAS INFORMED THAT IT WAS A NORMAL CHARACTERISTIC FOR THE VEHICLE. THE CONTACT FEELS THAT THE ISSUE WAS A SAFETY RISK BECAUSE A CRASH COULD OCCUR WHILE CROSSING AN INTERSECTION. THE CURRENT MILEAGE WAS 92,000 AND THE FAILURE MILEAGE WAS UNKNOWN.
Apr 09, 2009
DT: THE CONTACT STATED WHEN PRESSING THE GAS PEDAL THE VEHICLE HESITATED. THE VEHICLE HAS BEEN TO THE DEALER FIVE TIMES. THE DEALER REPLACED THE EXHAUST SENSOR, THE TURBO, AND REPROGRAMMED THE COMPUTER THREE TIMES. THE REPLACEMENT OF THESE PARTS HAD NOT CORRECTED THE PROBLEM. IT RECURRED INTERMITTENTLY. AT TIMES, IT SEEMED AS IF THE ENGINE WAS NOT RECEIVING A FUEL SUPPLY. INDICATOR LIGHTS DID NOT ILLUMINATE ON THE DASHBOARD. *AK
Oct 28, 2005
2005 FORD F350 HESITATED DURING ACCELERATION.*MR *NM
Aug 30, 2005
2003 FORD F350 DEVELOPED PROBLEMS WITH THE ACCELERATOR PEDAL.***NO ANSWER REQUIRED***. *MR WHEN THE GAS PEDAL WAS PRESSED THE VEHICLE WOULD NOT MOVE. EACH TIME THE VEHICLE WAS TAKEN TO A DEALER BUT THEY WERE UNABLE TO PERMANENTLY RECTIFY THE PROBLEM. VARIOUS COMPONENTS WERE REPLACED/REPAIRED BUT THE PROBLEM RECURRED. *NM
Aug 12, 2005
+ 7 more complaints for this component
ELECTRICAL SYSTEM
9 complaints
TL* THE CONTACT OWNS A 2003 FORD F-350. THE CONTACT STATED THAT AFTER REMOVING THE KEY FROM THE IGNITION SWITCH, THE ENGINE CONTINUED TO OPERATE ERRONEOUSLY. AFTER REINSERTING THE KEY INTO THE IGNITION THE CONTACT WAS ABLE TO SHUT THE ENGINE OFF. THE CONTACT STATED THAT THE FAILURE RECURRED MULTIPLE TIMES. THE CONTACT ALSO INDICATED THAT WHILE ATTEMPTING TO START THE VEHICLE THE KEY WOULD SPORADICALLY BECOME STUCK IN THE IGNITION SWITCH OR SHE WOULD BE UNABLE TO TURN THE IGNITION SWITCH TO START THE VEHICLE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE VIN WAS NOT AVAILABLE. THE FAILURE MILEAGE WAS 40,000.
Apr 10, 2014
TL* THE CONTACT OWNS A 2003 FORD F350. THE CONTACT STATED THAT THE ELECTRICAL SYSTEM FAILED AND WAS INOPERABLE. THE VEHICLE WAS TAKEN TO THE DEALER WHO ADVISED THAT THE AFTER MARKET RADIO COULD HAVE POSSIBLY CAUSED OTHER ELECTRICAL FAILURES WITHIN THE VEHICLE. THE MANUFACTURER WAS NOTIFIED AND A COMPLAINT WAS FILED BUT NO FURTHER ASSISTANCE WAS OFFERED. THE FAILURE MILEAGE WAS 155,000.
Oct 31, 2011
DT: WHEN THE CONSUMER WENT TO START THE VEHICLE IT WOULDN'T START. THE VEHICLE SAT FOR OVER 12 HOURS. IT HAD JUST COME OUT OF THE SHOP AND IT HAD A DOWN STRAP INSTALLED. THE FIRE STARTED IN THE RIGHT HAND SIDE OF THE DASHBOARD. ALL THE CONTENTS OF THE TRUCK WERE DESTROYED. BOTH THE POLICE AND FIRE DEP ARTMENT RESPONDED TO THE FIRE. *AK
Jun 30, 2005
Fire: 1
WHILE VEHICLE WAS PARKED A FIRE STARTED IN THE ENGINE COMPARTMENT. THE FIRE WAS PUT OUT. DEALERSHIP WAS NOTIFIED, BUT DID NOT RESOLVE THE PROBLEM. *AK
Jan 10, 2005
Fire: 1
WHILE DRIVING 30 MPH VEHICLE STALLED WITHOUT WARNING. THIS CAUSED LOSS OF STEERING AND BRAKES. DEALER REPLACED COMPUTER AND A COUPLE OF SENSORS, HOWEVER, PROBLEM STILL RECURRED. *AK
Apr 16, 2004
+ 4 more complaints for this component
TIRES
6 complaints
TL* THE CONTACT OWNS A 2003 FORD F-350 EQUIPPED WITH BF GOODRICH RUGGED TERRAIN T/A TIRES, SIZE: 285/75/16. WHILE DRIVING 75 MPH, THE FRONT PASSENGER SIDE TIRE SUSTAINED TREAD SEPARATION. THE CONTACT STATED THAT THERE WAS DAMAGE DOWN TO THE FENDER AND FENDER WELL OF THE VEHICLE. THE CONTACT STATED THAT THE TIRE WAS STILL FULLY INFLATED. THE CONTACT STATED THAT AAA WAS ABLE TO REPLACE THE TIRE, BUT ALL OF THE REMAINING TIRES ALSO SHOWED EVIDENCE OF TREAD SEPARATION. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE VIN AND DOT NUMBER WERE UNKNOWN. THE APPROXIMATE VEHICLE FAILURE MILEAGE WAS 150,000 AND THE TIRE FAILURE MILEAGE WAS 20,000.
May 05, 2017
TIRE WARPED WHILE DRIVING AT ABOUT 70 MPH. *TR
Jun 25, 2008
TL*THE CONTACT OWNS A 2003 FORD F350. WHILE DRIVING 65 MPH, THE FRONT PASSENGER SIDE AMERI-TECH TIRE BLEW OUT WITHOUT WARNING. THE CURRENT ESTIMATE FROM HIS INSURANCE COMPANY IS OVER $2,700, WHICH INCLUDES FENDER AND RIM DAMAGE ON THE FRONT PASSENGER SIDE, THE ABS SYSTEM, AND THE FENDER INNER-LINER. THE DOT NUMBER AND PURCHASE DATE WERE UNKNOWN. THE CURRENT MILEAGE IS 29,300 AND FAILURE MILEAGE WAS 29,100.
Jul 11, 2007
FAX FROM (FL) RE FOUR TIRE TREAD SEPARATIONS ON HIS 2003 FORD F350 4X4 LARIAT W/DUAL REAR WHEELS. *TS DOT NUMBERS ADOR 1P6 2202, ADOR 1P6 2802, ADOR 1P6 2202, ADOR 1P6 2202. THE FIRST TIRE TREAD SEPARATED AT 18000 MILES WHILE THE VEHICLE WAS BEING DRIVER AT 65 MPH. THE AWNING ON THE TRAILER BEING TOWED WAS DAMAGED. THE SECOND SEPARATION OCCURRED AT 20000 MILES, THE THIRD AT 24000 AND THE FOURTH AT 26000 MILES (CONTINENTAL GENERAL TIRES). *NM
Oct 26, 2006
LTR FM (FL) RE FOUR TIRE TREAD SEPARATIONS ON HIS 2003 FORD F350 4X4 LARIAT W/DUAL REAR WHEELS. *TS *JB
Aug 24, 2006
+ 1 more complaint for this component
SERVICE BRAKES, HYDRAULIC
5 complaints
2002 FORD F350 SUFFERED A RUPTURED BRAKE LINE.***NO ANSWER REQUIRED***. *MR WHEN THE BRAKES WERE APPLIED THE PEDAL DID NOT FEEL NORMAL. THE GARAGE FOUND THAT THE BRAKE LINE WAS IMPROPERLY INSTALLED. THE BRAKE LINE WAS RUBBING AGAINST THE SUPPORT FOR THE SHOCK ABSORBER. *SC *JB
Jun 08, 2005
PLOW AND SALT TRUCK FOR ROAD DEPARTMENT. HAS DUMP BOX INSTALLED. ANTI-LOCK BRAKES ACTIVATE PREMATURLY, EXTREMELY POOR STOPPING IN SNOWY CONDITIONS. FRONT END FEELS LIGHT AND "SQUIRLY" EVEN WITH EMPTY BED. WORKERS REFUSE TO OPERATE. DEEMED "UNSAFE". TOOK TO DEALER TWICE, THEY SAY BRAKES ARE OPERATING PROPERLY. VEHICAL HAS BEEN REPLACED AND IS FOR SALE.
Mar 24, 2005
Crash: 1
WHILE APPLYING THE BRAKES PEDAL WENT TO THE FLOOR. A LOUD NOISE CAME FROM THE PASSENGER'S SIDE WHEEL. CONSUME DROVE VEHICLE TO THE DEALER FOR INSPECTION, AND MECHANIC DETERMINED THAT THE BRAKE PADS AND THE ROTORS NEEDED REPLACED DUE TO CORROSION. *AK
Sep 21, 2004
WHILE APPLYING THE BRAKES,THE STEERING WHEEL VIBRATED UNCONTROLLABLY. THE DRIVER WAS ABLE TO MAINTAIN CONTROL OF THE VEHICLE AND DROVE IT HOME. THE DRIVER WILL CONTACT THE DEALER NEXT WEEK. PLEASE PROVIDE ANY ADDITIONAL INFORMATION. *NM
May 26, 2004
WHILE PULLING FROM A LIGHT OR STOP SIGN THE VEHICLE BRAKES WOULD LOCK UP WITHOUT WARNING. THE DEALERSHIP HAD BEEN CONTACTED. *NLM DURING STOP AND GO TRAFFIC, WHEN TRAFFIC OPENED UP THE BRAKES LOCKED UP AND WOULD STOP FOR 20 MINUTES AND UNLOCKED WHEN COOLED DOWN. AFTER THE SECOND TIME THE VEHICLE WAS TAKEN TO THE DEALER, THEY FOUND A DRAGGING PROBLEM. *SCC JB
Nov 12, 2003
STEERING
4 complaints
CONSUMER COMPLAINED ABOUT STEERING WHEEL LOCKING UP. VEHICLE WOULD TURN LEFT BUT WILL NOT TURN RIGHT. VEHICLE WAS TOWED TO THE DEALER, AND DEALER REPLACED THE STEERING GEAR BOX. CONSUMER HAS YET TO TEST DRIVE THE VEHICLE, HOWEVER, CONSUMER WANTED ON RECORD THAT THE STEERING BOX DEFECTION SHOULD BE LOOKED INTO. *AK
Jun 21, 2004
WHILE DRIVING 55 MPH THE VEHICLE'S STEERING FAILED WITHOUT WARNING. AS A RESULT THE DRIVER LOST CONTROL AND COLLIDED WITH A POLE. NO REPORT OF AIR BAG DEPLOYMENT. *NM
Feb 02, 2004
Crash: 1
THE STEERING COLUMN FAILED WHILE DRIVING AND CAUSED LOSS OF CONTROL. *NLM THE STEERING WHEEL HAD GONE AROUND IN A CIRCLE WITH NO RESPONSE. THE CONSUMER THEN TOUCHED THE BRAKES AND HAD GONE INTO A DITCH. SCC
Mar 20, 2003
Crash: 1
CONSUMER STATES THE BRAKE BOOSTER AND POWER STEERING PUMP ARE DEFECTIVE CAUSING THE BRAKE PEDAL TO LOCK UP AND/OR KICK BACK INTERMITTENTLY. TS
Dec 18, 2002
UNKNOWN OR OTHER
3 complaints
THE PASSENGER SIDE REAR SPARK PLUG BLEW OUT OF THE SOCKET
Oct 03, 2017
FOR SEVERAL YEARS, WE HAVE HAD EXHAUST GASES GOING INTO OUR TRUCK CAB. WE DO NOT DRIVE THE TRUCK DUE TO THIS REASON. ONE YEAR AGO, WE TOOK THE TRUCK TO DIESEL SPECIALISTS HERE IN LAS VEGAS. THEY SAID THAT THERE WAS A PROBLEM WITH THE MANIFOLD. THEY TRIED TO FIX IT AND IT WAS GOOD FOR ABOUT A WEEK UNTIL IT STARTED TO FORCE EXHAUST GASES BACK INTO THE CAB OF THE TRUCK. I UNDERSTAND THAT THERE IS A LARGE RECALL OF FORD VEHICLES DOING THE SAME ISSUE. IT APPEARS THAT FORD IS STILL MAKING VEHICLES WITH FAULTY EQUIPMENT ON THEM. WE WOULD HAVE TAKEN OUR TRUCK BACK TO THE DEALER BUT WE DO NOT HAVE A WARRANTY.
Aug 04, 2017
ON DECEMBER 7 2003, OUR 2003 FORD 350 TRUCK WHILE DRIVING DOWN THE ROAD AT 55 MILES AN HOUR, PULLED SHARPLY TO THE LEFT CAUSING US TO SPIN OUT OF CONTROL. WE HIT A DITCH ON THE LEFT SHOULDER OF THE ROAD, CAUSING THE TRUCK TO FLIP OVER ONTO THE RIGHT SIDE. WE ENDED UP IN THE MIDDLE OF ALMOND TREES. WE HAD OUR 1 YEAR OLD GRANDDAUGHTER WITH US. WE'VE INFORMED FORD IT WAS A MECHANICAL PROBLEM, BUT AS YET ALL THEY'VE DONE IS START THE BODY WORK. WE WOULD LIKE TO KNOW WHAT CAUSED THE TRUCK TO GO OUT OF CONTROL. WE FEEL LUCKY THAT WE WEREN'T KILLED OR THAT WE DIDN'T CAUSE THE DEATH OF ANOTHER FAMILY. WHAT WORRIES US IS WHAT ABOUT THE NEXT TIME, WILL WE ALL BE SO LUCKY. *LA
Dec 25, 2003
Crash: 1
Injuries: 1
AIR BAGS
3 complaints
TL* THE CONTACT OWNS A 2003 FORD F-350. WHILE DRIVING 50 MPH, THE CONTACT CRASHED INTO ANOTHER VEHICLE. NONE OF THE AIR BAGS DEPLOYED. THE VEHICLE WAS TOWED TO A COLLISION CENTER AND THE DEALER WAS NOT CONTACTED AS OF YET. A POLICE REPORT WAS FILED. THE CONTACT SUSTAINED A NECK FRACTURE THAT REQUIRED MEDICAL ATTENTION. THE MANUFACTURER WAS NOT CONTACTED. THE APPROXIMATE FAILURE MILEAGE WAS 147,000.
Aug 31, 2017
Crash: 1
Injuries: 1
TL* THE CONTACT OWNS A 2003 FORD F-350. THE CONTACT STATED THAT HE FELL ASLEEP WHILE DRIVING AND THE VEHICLE TRAVELED OFF THE ROADWAY WHERE HE CRASHED INTO TWO TREES. THE AIR BAGS DID NOT DEPLOY. THE CONTACT WAS UNINJURED AND A POLICE REPORT WAS FILED. THE VEHICLE WAS DESTROYED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VIN WAS UNAVAILABLE. THE CURRENT AND FAILURE MILEAGE WAS 140,000.
Apr 06, 2011
Crash: 1
THE CONSUMER'S VEHICLE WAS INVOLVED IN A FRONT END COLLISION WHILE DRIVING 50 MPH. UPON IMPACT, THE FRONT AIR BAGS DID NOT DEPLOY. PASSENGERS IN THE REAR SEATS SUSTAINED MINOR INJURIES. THERE WAS NO INDICATION THAT THERE WAS A PROBLEM WITH THE AIR BAGS PRIOR TO THE COLLISION. *AK THE VEHICLE WAS A TOTAL LOSS. THE FRONT SEAT PASSENGER'S AIR BAG DEPLOYED PREMATURELY. *SCC *JB
Nov 05, 2003
Crash: 1
Injuries: 2
ENGINE
3 complaints
DRIVING ALONG LOUD NOISE PULLED OVER TO FIND A SPARK PLUG BLEW OUT OF THE ENGINE BLOCK TAKING THE THREADS WITH IT. NO FIRE THANK GOODNESS!
Sep 26, 2016
I CALLED FORD MOTOR COMPANY MY 2003 FORD F350 SD. SC. 4X4 5.4 ENG. WITH THE PROBLEM WITH BOTH EXHAUST MANIFOLDS ROTTING AWAY & THE STUDS & NUTS THAT HOLD THE EXHAUST MANIFOLDS TO ENGINE HEADS THAT THEY WERE ALL ROTTING AWAY , THEY TOLD ME WE WON'T FIX THE PROBLEMS FOR FREE . I WOULD LIKE FOR TO INVESTIGATE THIS PROBLEM BEFORE MANY PEOPLE WILL GET INJURY OR MANY FATALITY WILL HAPPEN WHEN THE EXHAUST MANIFOLDS FALL OFF AND CATCH ON FIRE & BURN UP BECAUSE FIRE COMES OUT OF THE ENGINE TO THE EXHAUST MANIFOLDS . I TALKED TO MANY FORD DEALERS THEY TOLD ME THAT THEY HAVE REPLACED MANY OF THESE EXHAUST MANIFOLDS WITH THE SAME PROBLEMS I HAVE & HAD TO CHARGE THE OWNER OF THESE TRUCKS & MANY OTHER YEARS OF THESE FORD TRUCKS . PLEASE HELP ME & MANY OTHER OWNERS OF THESE FORD TRUCKS TO MAKE FORD MOTOR COMPANY RECALL THIS PROBLEMS BEFORE PEOPLE WILL DIE & FIX THIS PROBLEM FOR FREE . THANKS *TR
Jul 02, 2014
TL* THE CONTACT OWNS A 2003 FORD F-350. THE CONTACT STATED THAT THE ENGINE COOLANT LEVEL WAS FOUND TO BE PREMATURELY LOW. THE VEHICLE WAS TAKEN TO THE DEALER FOR INSPECTION, WHO ADVISED THE CONTACT THAT THE HEAD GASKET HEAD BOLTS WERE DEFECTIVE. THE MANUFACTURE WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGE WAS 130,000.
Oct 04, 2013
FUEL SYSTEM, DIESEL
3 complaints
HAVE FICM FAILURE AND MULTIPLE FUEL INJECTORS FAIL, WHEN TOOK TO DIESEL SHOP WAS INFORMED THAT THIS IS COMMON FAILURE AND THEY HAD AT LEAST 6 IN REPAIR SHOP WITH SAME PROBLEM. *TR
Apr 12, 2012
STRONG DIESEL FUEL ODOR AT IDLE IN CAB WITH WINDOWS CLOSED. STRONG DIESEL ODOR AROUND FRONT OF TRUCK. NO VISIBLE LEAKS OR DAMP AREAS. FEAR FIRE HAZARD. *TR
Mar 28, 2012
WHEN THE CONSUMER STARTED THE VEHICLE DIESEL FUEL FLOWED INTO THE CRANK CASE. THERE HAS BEEN AN EXPLOSION IN THE ENGINE COMPARTMENT OF THE VEHICLE. WHEN FUEL FLOWED INTO THE CRANK CASE THE ENGINE COULD NOT BE SHUT OFF UNTIL THE FUEL WAS EXHAUSTED. THE DEALER HAS SINCE FIXED THE PROBLEM.*AK
Sep 08, 2003
Fire: 1
FUEL/PROPULSION SYSTEM
2 complaints
VEHICLE STALLED AT 55 MPH ON HIGHWAY. *TR
Jan 20, 2015
TL* THE CONTACT OWNS A 2003 FORD F-350. THE CONTACT STATED THAT SMOKE BEGAN EMERGING FROM UNDER THE HOOD. THE CONTACT TOOK THE VEHICLE TO THE DEALER FOR INSPECTION WHERE THEY STATED THAT THERE WAS A HOLE IN THE FUEL LINE AND DIESEL FUEL HAD LEAKED ONTO THE ENGINE. THE DEALER STATED THAT THE FUEL LINE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 158,057.
Jul 18, 2013
Fire: 1
STRUCTURE
2 complaints
TL* THE CONTACT OWNS A 2003 FORD F-350. THE CONTACT STATED THAT THE BED OF THE VEHICLE WAS RUSTED AND CAUSED SHARP EDGES TO DEVELOP. THE CONTACT WAS UNABLE TO UTILIZE THE BED. THE VEHICLE WAS NOT REPAIRED AND THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 80,000.
Sep 11, 2014
DRIVER SIDE DOOR MOLDING IS SEPARATING FROM THE BODY OF THE VEHICLE AND COMING IN CONTACT WITH "THE FRONT FENDER". THE CONTACT OF THE MOLDING TO THE FENDER IS CAUSING AN OBSTRUCTION THAT CAUSES THE DOOR TO BE INOPERATIVE. DRIVER IS UNABLE TO OPEN THE DOOR. *AK
Aug 20, 2003
SUSPENSION
2 complaints
CONSUMER STATES: THE CONSUMER HEARD A SQUEAKING AND CLUNKING NOISE FROM THE BALL JOINTS WHILE TURNING CORNERS. THE BALL JOINTS FAILED BECAUSE THERE WERE NO GREASE FITTINGS. THE DEALER INSTALLED NEW BALL JOINTS AND GREASE FITTINGS. *NM
May 05, 2005
WHILE DRIVING, THE CONSUMER HEARD A LOUD GRINDING NOISE COMING FROM THE REAR END. PLEASE PROVIDE MORE INFORMATION. *JB
May 18, 2004
SEAT BELTS
2 complaints
WHILE DRIVING THE PASSENGER AND DRIVER FRONT SEAT BELTS LOCKED, RESTRAINING THE DRIVER, EVEN WHEN DRIVING AT A CONSTANT SPEED. THE CAUSE HAS NOT BEEN DETERMINED AT THIS TIME. THE DRIVER WILL CONTACT THE DEALER. *AK
Mar 02, 2005
THE REAR SEAT BELT BUCKLES WERE REPLACED WITH BUCKLES THAT EXTENDED EIGHT TO TEN INCHES. WHEN THE SEAT BELTS WERE USED THE BUCKLES WERE POSITIONED ON PASSENGER'S ABDOMEN WHICH COULD HAVE CAUSED SEVERE PROBLEMS DURING A COLLISION. *AK
Oct 06, 2003
FUEL SYSTEM, GASOLINE
2 complaints
CONSUMER STATED WHILE DRIVING AT 65-70 MPH VEHICLE SUDDENLY LOST POWER AND SHUT DOWN. CONSUMER TOOK THE VEHICLE TO THE DEALER, AND HAD THE PROBLEM RESOLVED BY REPLACING THE FUEL INJECTION SYSTEM. CURRENTLY, DEALER INDICATED THAT THE SENSORS WERE DEFECTIVE. VEHICLE WAS BACK AT THE DEALER FOR FURTHER EVALUATION. *AK THE VEHICLE HAS BROKEN A TOTAL OF 5 DIFFERENT TIMES AS A RESULT OF THIS PROBLEM. *NM
Jul 14, 2004
VEHICLE FAILS TO START BECAUSED THE ENGINE HAS A PINCHED O-RING.*AK
Jul 07, 2003
ENGINE AND ENGINE COOLING,FUEL SYSTEM, GASOLINE
2 complaints
WHILE DRIVING VEHICLE STALLED. DEALERSHIP INDICATED THAT THIS WAS DUE TO A MALFUNCTION IN THE FUEL INJECTORS. THE FUEL INJECTORS WERE REPLACED 8 TIMES, AND THE EGR VALVE WAS REPLACED TWICE. *AK
Mar 04, 2004
CONSUMER STATED WHILE DRIVING AT 60 MPH, THE VEHICLE STARTED SMOKING AND RATTLING. AFTER PULLING OVER TO THE SHOULDER TO INVESTIGATE THE PROBLEM, THE VEHICLE FAILED TO RESTART. AFTER TAKING THE VEHICLE TO THE DEALER, IT WAS FOUND THE FUEL INJECTOR WAS FAULTY AND THE ENGINE FAILED. THERE WERE NO INDICATION LIGHT ON AT ALL. *PH ALL ACCOUNTS TOOK PLACE APPROX. 11:30 P.M. ON AN EXTREMELY BUSY FREEWAY. AS OF 08/20/03, FORD HAD NOT COMPLIED WITH EITHER REPLACING THE ENGINE OR VEHICLE. *PH ALSO THE CONSUMER STATED THE COOLANT WAS LOW, AND THERE WAS STEAM COMING FROM UNDER THE HOOD. *JB
Sep 12, 2003
STEERING,ELECTRICAL SYSTEM,ENGINE
1 complaint
The wires for the camshaft position sensor are failing just like they have in others models of the f series and cause the truck to suddenly die while driving. There was already a recall in place but it doesn't cover this vin and so I would like to request the recall be extended to this trucks vin
Sep 20, 2021
STEERING,SERVICE BRAKES,ENGINE
1 complaint
AS I AM SURE YOU MUST BE AWARE OF THIS ISSUE: I PURCHASED USED A 2003 FORD -F350. I HAD MANY ISSUES AND HAD WORKED MOST OF THEM OUT. THERE WERE MANY ISSUES THAT WERE POSSIBLE I WAS CLEARLY UNAWARE OF. ONE BEING OF UTMOST SAFETY TO MYSELF AND OTHERS. MY HIGH PRESSURE OIL PUMP LOCATED INSIDE THE ENGINE OF MY 2003 FORD F-350 6.0 DIESEL FAILED. WHEN THAT HAPPENS THE ENGINE STOPS. THE HIGH PRESSURE OIL PUMP PROVIDES NEEDED PRESSURE TO THE INJECTORS IN ORDER TO HAVE A RUNNING ENGINE. BEING PARKED AND THE HPOP FAILING IS ONE THING HOWEVER DRIVING 55MPH ON A 2 LANE HIGHWAY AGAINST ONCOMING TRAFFIC ON A TURN IS A VERY BAD SITUATION. I AM FORTUNATE THAT I AM STILL VERY STRONG AT THE AGE OF 54. MY HPOP FAILED GOING 55MPH ON A LONG LEFT HAND TURN. AS THE ENGINE SHUTS DOWN BY BRAKES ARE LIMITED TO A SMALL AMOUNT OF STORAGE AND THEN THEY FAIL. THE STEERING HOWEVER FAILS IMMEDIATELY. I WAS HEADING STRAIT HEAD ON I TO A TRACKTOR TRAILER RIG. IT TOOK EVERY OUNCE OF STRENGTH TO ATTEMPT TO STEER THIS VEHICLE OUT OF THE OTHER LAND AND BRAKE GETTING IT OFF THE ROAD ASAP. IF THE BIG RIG HAD NOT MADE AN ATTEMPT TO MISS ME, I WOULDNT BE SENDING THIS LETTER. I WONDER HOW MANY OTHER PEOPLE HAD NOT THE STRENGTH TO STEER OUT OF A SITUATION OR HAVE TIME TO STOP AND WERE KILLED. THE REPORT MOST LIKELY SAID" DRIVER FELL ASLEEP." OR SOMETHING TO THAT AFFECT. THERE IS NO WAY THIS ENGINE SHOULD BE ALLOWED TO CONTINUE OPERATION ON THE ROAD PERIOD. FORD SHOULD HONOR ALL CURRENT OWNERS OF THIS VEHICLE WITH A VERY REASONABLE SETTLEMENT NOT TO MENTION HAVING A FORMAL INVESTIGATION INTO THIS MATTER. I KNOW OF NO OTHER VEHICLES ON THE ROAD THAT HAVE SUCH AN ISSUE. COMPLETE FAILURE OF STEERING AND BRAKES DUE TO AN UNFORESEEN INTERNAL MECHANICAL ISSUE IS A VERY POOR DESIGN. RUNNING OUT OF FUEL IS ONE THING, HOWEVER RUNNING OUT OF CONTROL IS ABSURD. HAD I KNOW WHO TO WRITE TOO SOONER I WOULD HAVE.
Jan 05, 2021
ENGINE,FUEL/PROPULSION SYSTEM
1 complaint
JUST DRIVING ON HIGHWAY 41 AND IT JUST STOPPED. ENGINE WENT DEAD. PULLED OVER TO SIDE OF ROAD AND TRIED STARTING AGAIN AND IT WOULDNT START. HAD TO GET IT TOWED. ITS BEEN IN SHOP FOR 20 DAYS. NEEDS A NEW FUEL TANK BECAUSE THE INNER LINING IS PEELING AND PARTICLES ARE GOING THROUGH ENGINE! NEED HELP I PURCHASED THIS TRUCK IN 2015 AND ITS BEEN IN SHOP 7 DIFFERENT TIMES.
Nov 12, 2019
EXTERIOR LIGHTING
1 complaint
MY DOME AND RUNNING BOARD LIGHTS ON MY 2003 FORD F350 SUPER DUTY, 4 DOOR TRUCK, STAY ON WHEN I AM DRIVING AND WHEN THE VEHICLE IS TURNED OFF AND LOCKED. ALSO WHILE DRIVING, THE DASH VEHICLE LIGHT IS RED SHOWING THAT ALL 4 DOORS ARE OPEN. ICAN BE PARKED OR MOVING, THE LIGHTS STAY ON. BOTH MY BATTERIES DRAIN. SO I HAV TO CARRY JUMPER CABLES.
Jul 16, 2019
TIRES,WHEELS
1 complaint
I AM INTERESTED IN THE HISTORY OF BF GOODRICH RUGGED TERRAIN T/A TIRES MADE IN 2014. I BOUGHT A SET OF FOUR LT 265/75-16 LRE FOR MY F350 ON 31 MAY, 2014. THEY CAME WITH A 6 YEAR/50K MILE WARRANTY. I HAD TIRES ROTATED PER WARRANTY. ON 11 APRIL, 2019, I EXPERIENCED A DRIVERS REAR TIRE FAILURE ON THE FLORIDA TURNPIKE (WITH CRUISE CONTROL SET @ 77MPH) CAUSING MINOR DAMAGE. CONTACTED DEALER WHO SAID "ROAD HAZARD" NOT COVERED. CONTACTED BFG WHO REQUESTED TIRE REMAINS BE SENT FOR ANALYSIS (TO PROVE ROAD HAZARD). ON 10 MAY DEPARTED FROM HOME TO GO TO VIRGINIA. 150 MILES UP I75 HAD TIRE VIBRATION AGAIN. PULLED OVER IN TIFTON, GA AND CHECKED TIRE TIME WITH IR GUN. ALL TIRES RUNNING BETWEEN 95-108 F. FELT TIRES AND HAD A BULGE IN DRIVERS FRONT. INSTALLED SPARE AND STARTED LOOKING FOR A BFG DEALER THAT HAD TWO TIRES IN INVENTORY (ONE TO INSTALL/ONE TO CARRY IN CASE OF FURTHER TROUBLE WITH SET). AS I APPROACHED MACON, GA, ANOTHER TIRE STARTED VIBRATING. WITHIN 5 MILES - IT BLEW HARD AT THE DRIVERS REAR POSITION AGAIN CAUSING OVER $3200 DAMAGE. CALLED EMERGENCY TIRE SERVICE AND REPLACED THE THREE REMAINING TIRES FROM THE 2014 SET. NOTIFIED BFG AND THEY ONLY WANTED THE THIRD FAILURE (SECOND BLOW) FOR ANALYSIS. CUSTOMER SERVICE REP STATED ALL TIRE BULGES ARE CAUSED BY "ROAD HAZARDS". IN SUMMARY - I EXPERIENCED THREE FAILURES IN JUST OVER 800 MILES ON A SET OF TIRES THAT ONLY HAVE 17,000 MILES ON THEM (REMAINING TREAD IS 11/32 PER DEALER INSPECTION). SINCE I STILL HAVE ALL OF THE TIRES - PHOTOS AVAILABLE UPON REQUEST. FIRST TIRE DID SHOW ONE SECTION 7 INCHES LONG WITH FOUR RADIAL SPLITS STARTING AT THE RIM. SECOND TIRE HAS NUMEROUS RADIAL SPLITS BUT NONE ARE CLOSELY CLUSTERED. IS MY EXPERIENCE UNIQUE TO MY SET OF CONDITIONS OR ARE THERE OTHER SIMILAR OCCURRENCES. THANK YOU FOR ANY HELP OR INSIGHT YOU CAN PROVIDE (XXXXX) PARTS OF THIS DOCUMENT HAVE BEEN REDACTED TO PROTECT PERSONALLY IDENTIFIABLE INFORMATION PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6).
Jun 27, 2019
POWER TRAIN,ENGINE
1 complaint
I WAS DRIVING DOWN THE ROAD AND I HEARD A LOUD POP. THE ENGINE HAD A VERY ABRUPT LOSS IN POWER AND BEGAN SHAKING AS I TRIED TO ACCELERATE. I WAS ON A 2 LANE ROAD AND HAD NO CHOICE BUT TO TRY AND MAINTAIN MY SPEED TO PREVENT CAUSING AN ACCIDENT FROM BEING REAR ENDED. AFTER DRIVING SEVERAL MILES TO A PLACE I COULD SAFELY STOP, I CHECKED UNDER THE HOOD AN A SPARK PLUG HAD BEEN SHOT FROM THE ENGINE. AFTER REVIEWING THIS ON THE WEB, THERE ARE MANY COMPLAINTS LIKE MINE WHERE SPARK PLUGS WERE SHOT OUT OF ENGINES. NHTSA NEEDS TO EVALUATE THIS AS REVIEW. HAD THE ENGINE CAUGHT FIRE I WOULD NOT HAVE KNOWN AND I HAD NO WHERE TO PULL OFF THE ROAD. THIS IS A RESULT OF AN CYLINDER HEAD WITH INADEQUATE THREADS FOR SPARK PLUGS TO THREAD INTO AND TAKE HOLD OVER TIME THE ALUMINUM WEAKENS AND THIS HAPPENS. IF THIS WASN'T A PROBLEM WHY DID FORD REDESIGN CYLINDER HEADS AFTER THESE MODEL ENGINES TO ACCOMMODATE MORE THREADING TO HOLD THE SPARK PLUGS IN THE ENGINE?
May 26, 2015
SERVICE BRAKES
1 complaint
I THOUGHT MY FOOT SLIPPED OFF THE BRAKE AND TAPED THE REAR END OF THE CAR IN FRONT OF ME. SCRATCHED THE BUMPER OF THE CAR I TAPPED. I WAS ON I 95S TOWARDS FREDERICKSBURG, VA WHEN MY BRAKE WARNING LIGHT CAME ON. TAPED BRAKE AND THE PEDAL ALMOST WENT TO THE FLOOR, BUT I DID HAVE SOME BRAKING. GOT THE TRUCK TO THE REPAIR SHOP, DIAGNOSED WILL HOLE IN BRAKE LINE CAUSED BY RUST. REPLACED 18 FT OF LINE. *TR
Jan 30, 2014
Crash: 1
POWER TRAIN
1 complaint
TL* THE CONTACT OWNS A 2003 FORD F350. THE CONTACT STATED THAT WHILE DRIVING 45 MPH THE TRANSMISSION STARTED SLIPPING AND THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT WAS ABLE TO RESTART VEHICLE. THE VEHICLE WAS NEITHER REPAIRED NOR TAKEN FOR DIAGNOSIS. THE MANUFACTURER WAS NOTIFIED OF INCIDENT. THE FAILURE MILEAGE WAS 47,000. *TR
May 07, 2013
LATCHES/LOCKS/LINKAGES
1 complaint
TL*THE CONTACT OWNS A 2003 FORD F350. WHILE PARKED AT A SHOPPING CENTER, THE CONTACT'S VEHICLE WAS BURGLARIZED AND ITEMS WERE STOLEN FROM WITHIN THE PASSENGER COMPARTMENT. A POLICE REPORT WAS FILED. SHE RESEARCHED AND DISCOVERED HOW EASY IT WAS FOR HER TYPE OF VEHICLE TO BE BURGLARIZED. SHE ALSO FOUND SEVERAL PEOPLE WHO EXPERIENCED THE SAME ISSUE. SHE TOOK THE VEHICLE TO THE DEALER AND SHOWED THEM THE BLACK CASING AROUND THE HANDLE OF THE PASSENGER SEAT. THE CASING WAS BENT, WHICH IS HOW IT WAS BURGLARIZED. THE DEALER STATED THAT THEY WERE AWARE OF THE FAILURE, BUT ALL THAT COULD BE DONE WOULD BE TO REPLACE THE DAMAGED LOCK WITH A NEW ONE. THE CURRENT AND FAILURE MILEAGES WERE 80,000. UPDATED 05/19/08 *BF UPDATED 05/19/08.
Apr 23, 2008
ENGINE AND ENGINE COOLING,POWER TRAIN
1 complaint
WHILE DRIVING 70 MPH, THE VEHICLE SHUT OFF. *AK THE REAR DIFFERENTAIL MADE A GRINDING SOUND AND SHUDDERED WHEN A TURN WAS MADE. *JB
Oct 26, 2004
AIR BAGS,VEHICLE SPEED CONTROL
1 complaint
WHILE DRIVING 20 MPH VEHICLE WAS ENGAGED IN FULL THROTTLE. THIS RESULTED IN UNEXPECTED ACCELERATION, ANDTHEN A COLLISION WITH A PARKED VEHICLE. NO REPORT OF AIR BAGS DEPLOYING. *AK
Oct 20, 2003
Crash: 1
SEATS
1 complaint
WHILE STOPPING AT A TRAFFIC LIGHT CONSUMER WAS REAR-ENDED BY ANOTHER VEHICLE. DRIVER'S SEAT HINGE BROKE, CAUSING IT TO COLLAPSE BACKWARD.*AK
Jul 23, 2003
Crash: 1
4.6/5.0
97 reviews

Frequently Asked Questions

How many problems does the 2003 FORD F-350 have?

The 2003 FORD F-350 currently has 88 owner-reported complaints according to NHTSA database. These complaints are organized by component to help identify common issues.

What are the most common problems with 2003 FORD F-350?

The most common problems reported for the 2003 FORD F-350 are organized by component above. Each component section shows owner-reported issues, crash reports, and fire incidents to help identify patterns and problem areas.

Where does this 2003 FORD F-350 problem data come from?

All problem and complaint data for the 2003 FORD F-350 comes directly from the National Highway Traffic Safety Administration (NHTSA) database. These are real complaints submitted by actual vehicle owners.

Other Years - FORD F-350

Other FORD Models

Similar Brands

← Back