292
Complaints Reported

Complaints by Component

ENGINE AND ENGINE COOLING
115 complaints
ENGINE FAILURE & OIL PRESSURE SENSOR WENT BAD.. *TR
Mar 09, 2009
1998 2.7 V-6 ENGINE IN DODGE STRATUS VEHICLE. OIL LIGHT CAME ON AND THEN THE ENGINE QUIT RUNNING. WHEN ATTEMPTING TO OBTAIN INFORMATION ON COST OF REPAIRS, I WAS TOLD BY MANY INDIVIDUALS THAT THIS ENGINE HAS FAILED IN THIS SAME MANNER FOR ALL OF THE VEHICLES. THE OIL WAS CHANGED EVERY 3000-5000 MILES, MORE OFTEN THAT SUGGESTED BY THE OWNERS MANUAL. THE OWNERS MANUAL STATES TO CHANGE IT EVERY 7500 MILES OR 6 MONTHS WHICH EVERY COMES FIRST. MOST OF THE REPAIR PLACES THAT I SPOKE TO SAID THAT THIS ENGINE SHOULD HAVE BEEN RECALLED DUE TO THIS FAILURE. *TR
Nov 05, 2008
WELL I HAVE HAD TO REPLACE MY OIL PRESSURE SENSOR ABOUT 6 TIMES ALREADY, IT SEEMS LIKE I REPLACE IT EVER 6 MONTHS OR SO, IT HAS BEEN LEAKING OUT OF THE ELECTRICAL END OF THE SENSOR BUT NEVER LEAKS OUT OF THE THREADED END THAT GOES INTO THE BLOCK, IT ALMOST CAUSED ME TO BLOW UP MY MOTOR THAT LAST TIME IT HAPPENED, IT IS JUST BECOMING A HUGE HASSLE THERE HAS TO BE SOME DEFECT IN THE PART, BECAUSE IT DOESN'T MATTER WHICH PARTS STORE I GO TOO THEY ALL END UP LEAKING. *TR
Sep 30, 2008
THROTTLE CABLE FRAYED AND STUCK IN CABLE HOUSING NOT LETTING THE ENGINE TO IDLE DOWN. *TR
Feb 18, 2008
1998 DODGE STRATUS CAUGHT FIRE UNDER THE HOOD. *KB OHIO TRAFFIC CRASH REPORT. *JB
Aug 28, 2007
Fire: 1
+ 110 more complaints for this component
SERVICE BRAKES, HYDRAULIC
33 complaints
I STARTED THE CAR, PLACED MY FOOT ON THE BRAKE AND IT WENT TO THE FLOOR. I EXITED THE VEHICLE AND FOUND A LARGE POOL OF FLUID ON THE RIGHT FRONT OF THE CAR. ABS AND BRAKE LIGHT CAME ON. MASTER CYLINDER WAS NEAR EMPTY. I HAD THE CAR TOWED TO MY LOCAL MECHANIC AND HE FOUND THAT ALL THE BRAKE LINES (6?) WERE LEAKING AT THE ABS PUMP. THIS IS THE CAR MY WIFE DRIVES. MY WIFE! I AM ANAL WITH REGARD TO MY VEHICLES CONDITION AND MAINTENANCE. TO HAVE A FAILURE LIKE THIS ON A WHAT IS SUPPOSED TO BE A "QUALITY AMERICAN MADE VEHICLE" IS ABSURD AND TOTALLY UNACCEPTABLE! MY BROTHERS 1999 HONDA, MY STEP SON'S 1991 NISSAN STANZA (RECENTLY SOLD) A 1993 GEO PRIZM (I.E. TOYOTA COROLLA!!!) RECENTLY SOLD HAD ZERO RUST ON ANY BRAKE FITTING, BRAKE LINE OR FUEL LINE. I HAD NO BRAKE ISSUES PREVIOUSLY. *KB
Dec 31, 2011
DT: THE CONTACT OWNS A 1998 DODGE STRATUS. THERE WERE TWO FIRES THAT ORIGINATED IN THE RIGHT REAR WHEEL. THE CONTACT STATED THE DEALERSHIP DID SOME WORK ON THE VEHICLE, AND WHEN HE GOT THE VEHICLE BACK HE HAD THE SAME PROBLEM. THE FIRES WERE DUE TO A MALFUNCTION IN THE ANTI-LOCK BRAKING SYSTEM. THE FIRES OCCURRED WHILE THE VEHICLE WAS IN MOTION. THE FIRST FIRE WAS ON JULY 2005, AND THE SECOND OCCURRED ON AUGUST 2005. *AK *JB
Oct 18, 2005
Fire: 1
SAFETY DEFECT IN 1998 *BF ON SEVERAL OCCASIONS EXTENDED STOPPING DISTANCE WAS EXPERIENCED RESULTING IN AN ACCIDENT. THE CONSUMER ADMITS THAT SHE MAY HAVE HIT THE GAS INSTEAD OF THE BRAKE WHILE ATTEMPTING TO STOP FOR A RED LIGHT. *TT CAMPAIGN ID NUMBER : 99V244000 *TC
Oct 28, 2004
Crash: 1
Injuries: 1
WHEN THE BRAKES WERE APPLIED VEHICLE DID NOT STOP, RESULTING IN A COLLISION. PRIOR TO THE COLLISION THE BRAKES FAILED, AND CONSUMER JUMPED A CURB, CONSUMER TURNED THE VEHICLE OFF, AND THAT STOPPED THE VEHICLE.*AK THE VEHICLE AIRBAG DID NOT DEPLOY. AS A RESULT OF THE COLLISION THE VEHICLE WAS DECLARED A TOTAL WRECK BY MET LIFE INSURANCE COMPANY. *TC
Sep 22, 2004
Crash: 1
Injuries: 1
BRAKES WENT OUT, AND PEDAL WENT ALL THE WAY TO THE FLOOR WHILE DRIVING. THISCOULD HAVE CAUSED AN ACCIDENT. CAUSE UNKNOWN. DEALER NOTIFIED.*AK
Jul 19, 2002
+ 28 more complaints for this component
POWER TRAIN
22 complaints
TL*THE CONTACT OWNS A 1998 DODGE STRATUS. THE VEHICLE WAS REPAIRED UNDER RECALL # 04V021000 (POWER TRAIN:AUTOMATIC TRANSMISSION:LEVER AND LINKAGE:FLOOR SHIFT). THE DEALER STATED THAT THE SHIFT LINKAGE CABLE WAS NOT A PART OF THE RECALL AND WILL NOT REPAIR THE VEHICLE FOR FREE. THE VEHICLE HAS NOT BEEN REPAIRED. THE PURCHASE DATE AND FAILURE MILEAGE WERE UNKNOWN. THE CURRENT MILEAGE IS 189,608.
Jun 18, 2007
I HAVE A 1998 DODGE STRATUS ES. THE TRANSMISSION WILL PLACE ITSELF IN NEUTRAL AT RANDOM TIMES WHILE AT A STOP. THE ONLY WAY TO GET THE TRANSMISSION WORKING AGAIN IS TO RESTART THE CAR. THE CAR HAS THE POWER-STICK TRANSMISSION. *NM
Nov 14, 2006
WE WERE JUST DRIVING ON THE HIGHWAY WHEN THE TRANSMISSION GAVE OUT (A COUPLE OF JERKS AND THEN NO ACCELERATION ABILITY). WE WERE ALMOST KILLED BY A SEMI WHO ALMOST RAN INTO US WHEN WE SUDDENLY AND DRASTICALLY SLOWED AND HADN'T BRAKED AND HE COULDN'T MOVE TO ANOTHER LANE BECAUSE OF OTHER TRUCKS IN THAT LANE. OUR 98 GRAND CARAVAN HAS ONLY 79K MILES ON IT AND THIS IS THE SECOND TRANSMISSION PROBLEM, (THOUGH I THINK THE FIRST TIME IT WAS REPAIRED RATHER THAN REPLACED TO THE TUNE OF $1000 AND JUST A COUPLE OF MONTHS PAST THE YEAR WARRANTY). NOW WE FIND THAT IT WILL BE $3000 TO REPLACE THE TRANSMISSION. WE HAVE IT SERVICED REGULARLY AT THE DODGE DEALER. WE HAVE ALSO HAD THE BATTERY REPLACED TWICE (ONCE WHEN THE FIRST TRANSMISSION PROBLEM WAS MIS-DIAGNOSED AS A FAULTY BATTERY). ALL WORK HAS BEEN OR IS BEING DONE BY THE DODGE DEALER. NOW I SEE ON THE INTERNET THAT THIS TRANSMISSION PROBLEM IS VERY COMMON WITH THIS MODEL. WHY ISN'T DODGE DOING SOMETHING ABOUT THIS INSTEAD OF GOUGING THE PUBLIC (NOT TO MENTION PUTTING US IN DANGER)?*JB
Dec 05, 2005
IN SEPTEMBER OF 2003 MY BROTHER THE ORGINAL OWNER OF THE 1998 DODGE STRATUS SOLD ME THE CAR. AND THEN RIGHT AFTER HE DIED. HE PURCHASED THE CAR 6 MONTHS BEFORE HE DIED IN MARCH 03. WHEN I RECEIVED THE CAR I TOOK IT TO THE SHOP TO GET AN OIL CHANGE AND THE TRANSMIISON FLIUD CHANGED. WHEN I DID THIS THE OIL MAN TOLD ME THAT I HAD NO OIL OR TRANSMISSON FLUID TO CHANGE IT HAD ALL LEAKED OUT. THE OIL MAN TOLD ME TO GET TO A MACHANIC AS SOON AS I COULD. I TOOK THE CAR TO GET IT FIXED AND THE AMCO TRANSMISSON PLACE CHAGED OVER 1,000.00 DOLLARS TO HAVE IT REPAIRED. I SEE THAT IT WAS 3 RECALLS ON THIS CAR AND ONE HAD TO DO WITH THE POWER TRAIN, AUTOMATIC TRANSMISSON/LEVEL AND LINKAGE. I CALLED DODGE AT THE NUMBER PROVIDED AND THEY TOLD ME THAT THE WARRANTY WAS UP AND THAT IF I HAD AREADY PAID TO GET THESE THING FIXED IT WOULD NOT BE REFUNDABLE.THE TRANSMISSON FLIUD HAD ALL LEAKED OUT THAT I HAD TO ALMOST REDO THE HOLD ENGINE. I DONOT HAVE THE OLD PARTS BUT I DO HAVE THE RECEIPT OF REPAIRS DONE.
May 17, 2005
VEHICLE FIRE
May 09, 2005
Fire: 1
+ 17 more complaints for this component
SUSPENSION
14 complaints
LEFT FRONT UPPER BALL JOINT BROKE
Oct 02, 2016
TL* THE CONTACT OWNS A 1998 DODGE STRATUS. WHILE PERFORMING AN OIL CHANGE, THE CONTACT NOTICED THAT THE LOWER BALL JOINT AND CONTROL ARMS WERE RUSTED. THE CONTACT STATED THAT THE LOWER BALL JOINTS AND CONTROL ARMS WERE REPLACED FOUR MONTHS AGO. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 74,000.
Mar 06, 2015
TL*THE CONTACT OWNS A 1998 DODGE STRATUS. WHILE DRIVING 5 MPH THE CONTACT HEARD A LOUD NOISE COMING FROM THE FRONT PASSENGER'S SIDE WHEEL. THE CONTACT'S RELATIVE INSPECTED THE VEHICLE AND DETERMINED THE BALL JOINTS WERE BROKEN. THE DEALER HAS NOT DIAGNOSED THE VEHICLE. THERE WAS RECALL 97V201000 CONCERNING THE LOWER BALL JOINTS FOR 1997 VEHICLES. THE CONTACT STATED THAT THIS VEHICLE SHOULD BE INCLUDED IN THE RECALL. *AK
Apr 17, 2007
I BEGAIN TO HAVE A GRINDING NOISE WHEN I TURNED AND THEN, MY HALF-SHAFT FELL OUT OF MY TRANSMISSION, CAUSING ME TO HAVE TO REPLACE MY HALF SHAFT AND LOWER CONTROL ARM. THAT STUFF IS NOT CHEAP. *AK
Nov 08, 2004
CONSUMER COMPLAINED ABOUT A BALL JOINT PROBLEM. WHEN TURNING CORNERS HEARD A POPPING SOUND ON DRIVER SIDE. THIS ACTION OCCURRED AT ALL SPEEDS. *AK *NM
Apr 20, 2004
+ 9 more complaints for this component
AIR BAGS
13 complaints
CAR HIT TWICE BY DEER. ONCE ON THE LEFT FRONT AND ONCE ON THE RIGHT FRONT. BOTH TIMES GOING ABOUT 55 MILES PER HOUR OR LESS AND NEITHER TIME DID THE AIR BAGS GO OFF. ON 10-31-2005 I WAS IN AN ACCIDENT WHERE MY CAR WENT OFF THE ROAD, AT LESS THAN 55 MPH, DUE TO RAIN AND A CURVE I WAS GOING AROUND. THE IMPACT BROKE MY REAR AXLE, THEN THE BACK OF THE CAR SIDE SWIPED A TREE AND TORE OFF THE REAR BUMPER AND FLIPPED THE CAR ON THE PASSENGER SIDE, FLIPPED BACK RIGHT SIDE UP AND THEN INTO THE SIDE OF A SMALL HILL. NONE OF THESE TIMES DID ANY AIR BAGS GO OFF. *NM
May 22, 2006
Crash: 1
Injuries: 1
WHILE DRIVING 35 MPH VEHICLE WAS INVOLVED IN A HEAD ON COLLISION. THE DUAL AIRBAGS DEPLOYED WITHOUT AIR. AS A RESULT, DRIVER SUSTAINED SEVERE FACIAL INJURIES. *AK
Jan 09, 2004
Crash: 1
Injuries: 1
CAR CRACH
Nov 12, 2003
Crash: 1
ACCIDENT OCCURRED AND AIR BAGS DID NOT DEPLOY. DEALER HAS BEEN NOTIFIED. PH
Jan 29, 2003
Crash: 1
Injuries: 1
CONSUMER STATED THAT WHEN THEY WAS HIT IN THE FRONT CENTER OF THE VEHICLE THE AIR BAG DID NOT DEPLOY CAUSING MINOR INJURIES TO THE CONSUMER. DEALER NOTIFIES. TS
Jan 21, 2003
Crash: 1
Injuries: 1
+ 8 more complaints for this component
STEERING
12 complaints
TL* THE CONTACT OWNS A 1998 DODGE STRATUS. THE CONTACT STATED THAT THE VEHICLE WAS PARKED WHEN IT IGNITIED INTO FLAMES. THE FIRE DEPARTMENT WAS ABLE TO EXTINGUISH THE FIRE AND A FIRE REPORT WAS FILED. THE FIRE DEPARTMENT CONCLUDED THAT THE FIRE ORIGINATED FROM THE HIGH PRESSURE POWER STEERING HOSE. THE CONTACT SPOKE WITH THE MANUFACTURER AND WAS ADVISED THAT THE VEHICLE WAS NOT INCLUDED IN NHTSA RECALL CAMPAIGN ID NUMBER: 06V001000 (STEERING: HYDRAULIC POWER ASSIST: HOSE, PIPING, AND CONNECTIONS) DEALT WITH THE 1999-2002 DODGE STRATUS AND NOT THE 1998 EVEN THOUGHT THE FAILURE WAS CAUSED FOR THE SAME REASON. THE FAILURE MILEAGE WAS 175,000.
Jun 23, 2011
Fire: 1
POWER STEERING PRESSURE LINE LEAKING ON EXHAUST MANIFOLD FIRE RISK. *TR
Aug 12, 2009
1998 DODGE STRATUS ENGINE COMPARTMENT FIRE ASSOCIATED WITH POWER STEERING LEAKS. *TR
Jun 05, 2008
Fire: 1
CAR WAS LEAKING POWER STEERING FLUID SO WE KEPT ON ADDING MORE UNTIL WE COULD SAVE ENOUGH MONEY TO GET THE PROBLEM FIXED(AROUND $350.00, NO SMALL FEE FOR A WORKING FAMILY!)THEN, THE SMOKING GOT WORSE UNTIL ONE DAY IT JUST CAUGHT ON FIRE! I COULDN'T PUT IT OUT WITH AN EXTINGUISHER, THE FIRE DEPARTMENT HAD TO PUT IT OUT AND NOW THE CAR IS TOTALED! CAN WE STILL GET A RECALL? *TR
Dec 07, 2007
Fire: 1
CAR STARTED SMOKING UNDER THE HOOD AND THEN IT CAUGHT ON FIRE THE OWNER OF THE STORE HAD TO CALL THE FIRE DEPARTMENT. THE CAR IS NOT DRIVABLE AS EVERYTHING UNDER THE HOOD IS BURNT. *JB
Jan 11, 2006
Fire: 1
+ 7 more complaints for this component
SEAT BELTS
10 complaints
DRIVER'S SEAT BELT BUCKLE IS INOPERATIVE. THE BUCKLE DOES NOT LOCK. DRIVER CONTACTED THE DEALER, AND WAS INFORMED THAT THE BUCKLE NEEDED TO BE REPLACED. *AK....A PENNY WAS FOUND STUCK IN THE RECEIVER. ONCE REMOVED THE SEAT BELT PERFORMED PERFECTLY. *AK
Mar 25, 2005
I WAS IN A CAR ACCIDENT ON FEB. 16 1998/1999??. AND MY CAR WAS ALMOST TOTALLED. THE COLLISION REPAIR SHOP WAS SUPPOSED TO REPLACE ALL OF THE BAD PARTS TOTALLING SOMEWHERE A LITTLE OVER 9,000$ . EVERY TIME I WOULD GO TO PICK UP MY CAR THERE WAS SOMETHING WRONG WITH IT. FINALLY AFTER LIKE 5 TRIPS TO THE REPAIR SHOP I TOOK IT HOME. A WHILE LATER I HAD TAKEN IT IN TO BE WORKED ON THE SIDE THE DAMAGE WAS DONE TO IT. THE CHRYSLER DEALERSHIP TOLD ME THEY WOULD NOT TOUCH IT BECAUSE IT WAS A HAZARDOUS SITUATION AND THE CAR SHOULDN'T EVEN BE ON THE ROAD. WELL COME TO FIND OUT THE DAMAGE WAS NEVER REPLACED BUT BUFFED AND COATED WITH BONDO. THE COLLISION SHOP ENDED UP PAYING FOR IT TO GET FIXED BUT STATE FARM SAID HE WAS GUILTY OF INSURANCE FRAUD AND I WOULD LIKE THIS INVESTIGATED. IF HE HAS DONE IT TO ME HOW MANY OTHER PEOPLE HAS HE DONE IT TO. NOT TO MENTION THE FACT THAT EVERYONE INCLUDING MY 7 YEAR OLD NEPHEW, WAS IN DANGER EVERY TIME WE WOULD GET IN MY CAR. THEY SAID THAT IT WOULD BUCKLE UNDER THE LIGHTEST OF HITS. PLEASE GET BACK TO ME REGARDING THIS MATTER. THE COLLISION SHOP IS CALLED EXPERT COLLISION ON 14 MILE & DEQUINDRE/ JOHN R.*AK
Aug 20, 2002
Crash: 1
REAR SEATBELT WILL NOT BUCKLE,CAUSING IT TO BE USELESS IN EVENT OF A VEHICLE CRASH. CAUSE UNKNOWN.DEALER NOTIFIED. *AK
Jul 17, 2002
REAR SHOULDER BELTS WAS BEGINNING TO FRAY UNDER NORMAL USE. RIGHT REAR SHOULDER BELT WAS FRAYING MORE THAN THE LEFT SIDE, EQUAL USE ON EACH SIDE. DEALERSHIP INFORMED CONSUMER THEY CANNOT REPAIR AT NO COST TO CONSUMER BECAUSE IT WAS NO LONGER COVERED UNDER WARRANTY. PLEASE PROVIDE ANY ADDITIONAL INFORMATION/ATTACHMENTS. *AK
Apr 12, 2001
DRIVERSIDE SEATBELT WONT FULLY RETRACT AUTOMATICALLY. THE CLIP HAS BEEN SLAMMED IN THE DOOR SEVERAL TIMES NOW. *AK
Feb 08, 2001
+ 5 more complaints for this component
ELECTRICAL SYSTEM
8 complaints
DT*: THE CONTACT STATED WHILE PULLING INTO A PARKING LOT, SMOKE WAS NOTICED COMING FROM UNDER THE HOOD. THE FRONT HOOD WAS RAISED, AND FLAMES WERE NOTICED ON TOP OF THE ENGINE. THERE WAS NOTHING UNUSUAL ABOUT THE WAY THE VEHICLE HAD OPERATED PRIOR TO THE FIRE. THE FIRE DEPARTMENT WAS CONTACTED, AND EXTINGUISHED THE FIRE. THE TYPE OF FIRE AND EXACT COMPONENT INVOLVED WAS UNKNOWN. THE VEHICLE WAS TOWED TO A LOCAL DEALERSHIP, WHERE IT WAS DEEMED TOTALED. THE CONTACT PLANNED TO NOTIFY THE MANUFACTURER AFTER FILING A COMPLAINT WITH THE NHTSA. A POLICE REPORT WAS NOT TAKEN, BUT THERE WERE PICTURES AVAILABLE.*AK
Dec 06, 2006
Fire: 1
BATTERY LIGHT INDICATOR ON PANEL COMING ON/OFF LEADING TO LIGHT GLITCHES ON SPEED INDICATOR PANEL, RADIO CLOCK, INTERIOR LIGHTS, HEADLIGHTS, REAR DEFROST COMING ON BY ITSELF AND GLITCHING ON THE ODOMETER READING. CAR BATTERY SHOWING 11 VOLTS OUT OF 12 FOR COLD START AND ALTERNATOR ALREADY CHANGED OUT HAVE RECEIPT TO SHOW THIS PAST MONTH.*AK
Jan 06, 2005
WHILE PLACING THE KEY INSIDE THE IGNITION VEHICLE FAILED TO TURN ON ITS OWN. CONSUMER CONTACTED THE DEALER FOR INSPECTION, AND DEALER INFORMED CONSUMER THAT THE VEHICLE HAD TO BE TOWED FOR SERVICE. *AK
Nov 10, 2004
HERBEE MOTORS 130 SUNRISE HIGHWAY WEST ISLIP N.Y. 11795 AUGUST 15, 2004. *JB ATTN. SERVICE MANGER, THE PREVENTATIVE RECALL WORK DONE ON MY 1998 DODGE STRATUS IS UNSAFE AND TOTALLY UNACCEPTABLE. PLEASE SEE SERVICE HISTORY FOR AUG. 12 AND AUG. 13, 2004 AND REFER TO YOUR INVOICE DOCS27685 DATED 8/13/04 VIN [XXX] FOR RECALL C45 FLOOR SHIFTER IGNITION PARK INTERLOCK. I PICKED UP MY CAR FRIDAY EVENING AUG 13. AFTER PARKING MY CAR (PLACING THE SHIFT IN THE PARK POSITION WITH THE HAND BRAKE ON) I WAS UNABLE TO REMOVE THE KEY FROM THE IGNITION. I DROVE BACK TO HERBEE MOTORS AND SAW YOUR MANAGER CHARLIE WHO ASSISTED ME. AT FIRST HE WAS UNABLE TO REMOVE THE KEY WITH THE CAR SHIFT IN THE PARKED POSITION. THEN AFTER NUMEROUS ATTEMPTS HE WAS ABLE TO REMOVE THE KEY AND ADVISED ME TO BRING THE CAR BACK ON MONDAY FOR SERVICE. I STARTED MY CAR AND SHUT IT OFF AND WAS ABLE TO REMOVE THE KEY WITH NO EFFORT (LIKE NORMAL) BUT THE DASH PARKING LIGHT AND ODOMETER LIGHT WERE STILL ON. THE KEY WOULD NOT TURN ALL THE WAY TO THE PARKED POSITION BUT WAS ABLE TO BE REMOVED. I SAW CHARLIE WHO VERIFIED THAT THE KEY WAS EASILY REMOVED BUT NOT GOING INTO THE LOCKED PARK POSITION. THE PROBLEM OF KEY REMOVAL APPEARS TO BE INTERMITTENT. AFTER ATTEMPTS, AGAIN HE WAS ABLE TO REMOVE THE KEY IN THE PROPER POSITION. HE THOUGHT THE HAND BRAKE HAD SOMETHING TO DO WITH THE KEY REMOVAL AND ADVISED NOT TO USE THE HAND BRAKE. THIS AFTERNOON AFTER RETURNING FROM SHOPPING I PARKED MY CAR ON MY DRIVEWAY AND THOUGHT I HAD PLACED THE FLOOR SHIFT INTO THE PARKED POSITION AND REMOVED THE KEY EASILY. I GOT OUT OF THE CAR BUT THE SHIFT WAS IN THE REVERSE POSITION AND MY CAR ROLLED DOWN MY DRIVEWAY INTO THE STREET. THE CAR COULD HAVE KILLED SOMEONE OR CAUSE SERIOUS PROPERTY DAMAGE VERY EASILY. [XXX]. *JB INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)
Aug 15, 2004
THE IGNITION KEY WAS STUCK IN THE "ON POSITION" AND COULD NOT BE REMOVED. THE CONSUMER CONTACTED THE MANUFACTURER AND THE DEALER BUT NO ASSISTANCE WAS OFFERED. *AK *SC *JB
Jul 30, 2004
+ 3 more complaints for this component
VEHICLE SPEED CONTROL
7 complaints
DT: THE CALLER'S SON WAS DRIVING AND WITHOUT WARNING THE THROTTLE STUCK. HE TRIED TO PULL THE FOOT PEDAL UP WITH HIS FOOT BUT IT DID NOT STOP THE VEHICLE. HE WENT THROUGH A STOP SIGN AND ALMOST LOST CONTROL OF VEHICLE, BUT FINALLY GOT THE VEHICLE TO STOP BY TURNING OFF THE IGNITION. THE CALLER SAID THE BRAKES WERE ON FIRE. THE FIRE DEPARTMENT WAS NOT CALLED. THE VEHICLE REACHED THE SPEED OF 80 MPH. DEALER HAS NOT BEEN CONTACTED YET. WILL TAKE VEHICLE TO HER OWN MECHANIC. MANUFACTURER SAID THERE WAS NO RECALL AND SHE SHOULD TAKE THE VEHICLE TO DEALER TO GET IT REPAIRED.*AK THE PROBLEM WAS THE CRUISE CONTROL MODULATOR. *JB
Sep 29, 2005
Fire: 1
DT: THE CONTACT STATED CRUISE CONTROL WOULD NOT GO OFF. THIS HAPPENED ON 8-26-05. SHE HAD THE CRUISE CONTROL WAS SET AT 60 MPH, BUT INSTEAD IT KEPT CLIMBING HIGHER. THE CONSUMER DID NOT HAVE ANY PROBLEMS WITH THE CRUISE CONTROL PRIOR TO THIS OCCURRENCE. THE SERVICE DEALER HAD TO CUT THE WIRES TO GET THE CRUISE CONTROL TO GO OFF. THE BRAKES WERE RUINED BECAUSE SHE HAD TO RIDE THE BRAKES FOR SO LONG. THE SERVICE REPAIR SHOP SAID THE MODULE TO THE CRUISE CONTROL WAS BAD. HE DISCONNECTED THE CRUISE CONTROL. HE TOLD HER TO CALL THE NHTSA AND REPORT THIS BECAUSE HE HAD NEVER SEEN ANYTHING LIKE IT. THE CONSUMER DID NOT HAVE THE MONEY TO HAVE THE MODULE REPLACED. THE CONSUMER FELT THAT SHE SHOULD BE REIMBURSED FOR THE COST INCURRED. *AK THE CONSUMER SHE IS EXPERIENCING BACK PAIN FROM BEING JERKED AROUND IN THE VEHICLE. *JB
Sep 29, 2005
Injuries: 1
BRAKES FAILED TO DISENGAGE THE CRUISE CONTROL SET AT 70 MPH. CONSUMER CONTINUED DEPRESSING BRAKE PEDAL UNTIL HE SMELLED RUBBER BURNING. WHEN THIS OCCURRED THE IGNITION SWITCH WAS IMMEDIATELY TURNED OFF. VEHICLE STARTED TO SLOW DOWN, BUT THE FAILURE CONTINUED WHEN THE IGNITION WAS TURNED BACK ON. IGNITION WAS THEN TURNED BACK OFF, AND VEHICLE COASTED TO THE MEDIAN. WHEN VEHICLE WAS AT A COMPLETE STOP CONSUMER PUT THE VEHICLE IN PARK BEFORE RESTARTING. CRUISE CONTROL DISENGAGED, AND THE FAILURE HAD CORRECTED ITSELF. DEALERSHIP WAS NOT NOTIFIED, THE CAUSE OF THE FAILURE WAS UNDETERMINED.*AK ...*AK
Sep 24, 2004
CONSUMER STATE THAT WHILE DRIVING ON THE NY STATE FOR ABOUT 2 1/2 HOURS, THE CRUISE CONTROL WAS SET AT 65 MPH, AS CONSUMER WAS PULLING INTO A PASSING LANE WITHOUT ACCELERATING TO PASS A SLOWER VEHICLE, THE SPEED JUMPED TO 80 MPH VERY RAPIDLY, CONSUMER THEN HIT THE ACCELERATOR TWO OR THREE TIMES WITHOUT ANY RESULTS THEN TURNED OFF THE CRUISE CONTROL AND THE SLOWED DOWN BACK TO NORMAL. *MJ
Jul 11, 2002
THROTTLE LINKAGES BROKE IN MECHANISM, CAUSING VEHICLE TO MOVE FULL FORCE. ENGINE MADE VEHICLE MOVE FAST AS OWNER WAS PRESSING ON BRAKES. CONSUMER THAN PLACED THE VEHICLE IN NEUTRAL AND EVENTUALLY TURNED OFF THE VEHICLE TO MAKE IT STOP.*AK
Mar 05, 2001
+ 2 more complaints for this component
UNKNOWN OR OTHER
6 complaints
THE FLOOR MAT ON THE DRIVER SIDE, SLID FORWARD AND BECAME TANGLED IN THE STEERING UNIVERSAL JOINT. THIS CAUSED THE STEERING WHEEL TO BE HARD TO TURN. *JB
May 20, 2003
IMPRESSED WITH THE SPORTY STYLE OF MY SISTER'S 4-DOOR DODGE STRATUS, I PURCHASED ONE FOR MY WIFE IN 1998 (A 1998 DODGE STRATUS). IT WASN'T LONG BEFORE MY SISTER BEGAN HAVING PROBLEMS WITH HER CAR. I BLAMED HER AND TOLD HER THAT SHE WAS TOO ROUGH ON HER CAR (SHE HAS A LEAD FOOT). MY WIFE AND I TAKE VERY GOOD CARE OF OUR CARS AND I WAS CONFIDENT WE WOULD NOT RUN INTO THE SAME PROBLEMS. WELL, RECENTLY I NOTICED THE PRESENCE OF A SMALL OIL-PUDDLE WERE MY WIFE KEEPS HER CAR. I LEARNED THAT THE HEAD GASKET WAS IN NEED OF REPLACEMENT. I'VE YET TO HAVE THIS DONE BUT WAS QUOTED AND ESTIMATE OF $700-750. THE MECHANIC INFORMED ME THAT THIS WAS A VERY COMMON PROBLEM FOR THE STRATUS. SO COMMON THAT HE PREDICTED THE DIAGNOSIS BEFORE EVER LOOKING UNDER THE HOOD. MY STRATUS ONLY HAS 55,000 MILES ON IT. ITS BEEN WELL MAINTAINED AND DRIVEN WITH CARE. TURNS OUT, MY SISTER HAD THE SAME PROBLEM (HEAD GASKET FAILURE) AT/NEAR 65,000 MILES. IN TYPING THE WORDS "DODGE STRATUS HEAD GASKET" IN AN INTERNET SEARCH MANY ARTICLES, COMPLAINTS, AND REVIEWS NOTED THIS ALL-TO COMMON PROBLEM. I ALSO LEARNED MANY OF THOSE WHO HAVE HAD THIS FAILURE RECEIVED ZERO TO LITTLE COMPENSATION/COMPASSION FROM THE MANUFACTUER FOR THE OBVIOUS DEFECT. IT APPAERS DODGE HAS IDENTIFIED THIS PROBLEM AND HAS RE-DESIGNED THE GASKET MULTIPLE TIMES. TWO SEPERATE MECHANICS INFORMED ME THAT I CAN HAVE THE GASKET REPLACED BUT I SHOULD EXPECT THE PROBLEM TO HAPPEN AGAIN SOON AFTER. THIS DOESN'T SEEM FAIR. I UNDERSTAND DEFECTS OCCUR BUT FEEL PEOPLE SHOULD BE COMPENSATED WHEN THEY DO. DODGE NEEDS TO STAND BEHIND THEIR PRODUCT AND ADMIT THEY ARE RESPONSIBLE. THIS DEFECT HAS LED TO MUCH FRUSTRATION.. A RESPONSE OF WHAT I SHOULD/CAN DO WOULD BE APPRECIATED
Feb 20, 2003
I HAVE A 1998 DODGE STRATUS WITH A 2.4L 4 CYLINDER ENGINE WITH 86,000+ MILES THAT HAS RECENTLY DEVELOPED A HEAD GASKET OIL LEAK. I AM AWARE THAT THIS IS A COMMON PROBLEM WITH THIS ENGINE AND THE ASSOCIATED TSB(09-05-98). WHEN I NOTICED THE LEAK, I TOOK MY CAR TO THE DEALER IN TOWN AND WAS TOLD THAT THE REGIONAL OFFICE DENIED MY REQUEST FOR PAYMENT OF THE REPAIR. I DID NOT HAVE THE REPAIR DONE, BUT GOT AN ESTIMATE FOR $800. NEXT, I CONTACTED THE CHRYSLER CUSTOMER SERVICE LINE IN DETROIT, MI.(1-800-992-1997). I WAS TOLD POLITELY THAT THEY WOULD LIKE TO HELP ME BUT THAT MY CAR WAS TOO FAR OUT OF WARRANTY AND THAT THERE WAS NO WARRANTY EXTENSION FOR THIS PROBLEM. I ASKED WHY SOME PEOPLE RECEIVED ASSISTANCE FOR THE SAME PROBLEM WHILE OTHERS DID NOT, AND WAS TOLD THAT "THIS OFFICE WOULD NOT HAVE AUTHORIZED THOSE PAYMENTS". I ASKED FOR A NUMBER OR ADDRESS TO MAKE AN APPEAL TO THIS DECISION AND WAS TOLD THAT THEY HAD ALREADY MADE THE FINAL DECISION, THERE WAS NO ONE ELSE TO APPEAL TO, AND THE DECISION WOULD NOT BE OVERTURNED.
Dec 11, 2002
NO SUMMARY
Sep 18, 2000
NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK
Jan 30, 2000
+ 1 more complaint for this component
VISIBILITY
5 complaints
DT: CONSUMER STATED THERE WAS A FIRE IN THE DRIVER'S SIDE DOOR PANEL. THE POWER WINDOWS DID NOT WORK. CONSUMER BELIEVED THIS WAS THE SOURCE OF THE FIRE. THE CAR WAS NOT DRIVABLE. TOOK IT TO A LOCAL DEALER. *AK
Jul 05, 2005
Fire: 1
HEATER CORE HAS FAILED AND CAUSES THE CAR TO OVERHEAT. THE DEFECTIVE HEATER ALSO CAUSES THE CAR INTERIOR TO FILL WITH STEAM. THIS ALSO CAUSES THE CAR TO STALL OUT UNEXPECTEDLY.*AK
Jul 26, 2001
THE DRIVER AND PASSENGER FRONT WINDOWS FAILED. *MJS
Dec 04, 2000
WHEN HEAT IS BEING USED WINDOWS AND WINDSHIELD FOG UP, CAUSING POOR DRIVER VISIBILITY. CONSUMER HAS CONTACTED DEALER, PLEASE PROVIDE ANY FURTHER DETAILS. *AK
Feb 23, 2000
POWER WINDOW SWITCH FAILED. *YC
Feb 01, 1999
SERVICE BRAKES, HYDRAULIC,AIR BAGS
4 complaints
30MPH FRONTAL CRASH, DRIVER'S/PASSENGER'S AIRBAGS DIDN'T DEPLOY, BRAKE PEDAL WENT TO FLOOR, BUT CAR DIDN'T RESPOND. *AK
Dec 20, 1999
Crash: 1
Injuries: 1
2ND ACCIDENT, BRAKE PEDAL WENT TO FLOOR, CAR DID NOT SLOWDOWN, DIRECT FRONAL IMPACT 45MPH, DRIVER'S & PASSENGER'S AIRBAGS DID NOT DEPLOY. *AK
Dec 20, 1999
Crash: 1
Injuries: 2
70 DEGREES, DRY LEVEL ROAD SURFACE, SLIGHT CURVE IN ROAD TO LEFT. FRONTAL IMPACT AT 40MPH INTO SIDE OF SECOND VEHICLE THAT RAN STOP SIGN. PRESSED BRAKE PEDAL WITH BOTH FEET AT MAXIMUM FORCE. BRAKE PEDAL WENT TO FLOOR AND CAR DID NOT SLOW OR STOP RESULTING IN IMPACT. NORMALY, ABS ACTIVATES AT THE SLIGHTEST SIGN OF ROAD IRREGULARITY. ABS SOUNDS NOT HEARD DURING ENTIRE INCIDENT. ABS PULSING SENSATION IN BRAKE PEDAL NOT FELT DURING ENTIRE INCIDENT. ALSO, FRONT DRIVER AND FRONT PASSENGER AIRBAGS DID NOT DEPLOY.
Sep 20, 1999
Crash: 1
WHENEVER BRAKES ARE APPLIED, THEY WOULD MAKE LOUD SQUEALING NOISES. THEY WOULD LET GO WHILE BEING PRESSED. REARENDED ANOTHER VEHICLE WHEN THE BRAKES FAILED TO WORK PROPERLY AT 60 MPH. AT TIME OF IMPACT, THE AIR BAGS DID NOT DEPLOY. *AK
Dec 09, 1998
Crash: 1
FUEL SYSTEM, GASOLINE
3 complaints
MY NAME IS [XXX] . THIS COMPLAINT IS FOR THE CAR ALLOWANCE REBATE SYSTEM. I FEEL THAT MY CAR IS ELIGIBLE FOR THE CLUNKERS FOR CASH PROGRAM. IT IS A CLUNKER, IT IS 11 YEARS OLD. BUT BECAUSE THE MPG IS 22 I WAS TOLD I DON'T QUALIFY. WHY HAVEN'T IT BEEN MADE A LITTLE EASIER FOR THOSE THAT OWN OLD VEHICLES PERIOD? I FEEL THIS ISN'T DONE FAIRLY AND IT COULD BE CHANGED. THIS WILL BE BREAK FOR THOSE WHO CAN'T AFFORD TO UPGRADE TO BETTER CARS. THOSE THAT ARE LOW INCOME WORKERS. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR
Jul 23, 2009
I AM FILING THIS COMPLAINT TO HAVE ON RECORD THIS INCIDENT AND SEEKING QUESTIONS ALREADY POSED TO DAIMLER CHRYSLER. I INFORMED DAIMLER CHRYSLER BY EMAIL, THAT MY 1998 DODGE STRATUS CAUGHT ON FIRE WITH MY DAUGHTER. ON MAY 23, 07 ON PEOPLES COURT A 1997 DODGE STRATUS WAS BURNT TO A CRISP BECAUSE OF THE POWER STEERING HOSE. A PORTER HILL @ 248-944-7134, FROM DAIMLER CHRYSLER CONTACTED ME REGARDING THE DATE THAT THIS INCIDENT TOOK PLACE AND THE LOCATION OF THE VEHICLE. THAT THEY WOULD BE COMING TO SEE THE VEHICLE. I JUST RECEIVED A LETTER TODAY FROM DAIMLER CHRYSLER CUSTOMER CLAIMS RESOLUTION GROUP WITH NO SIGNATURES READING THAT THEY HAVE COMPLETED THEIR INVESTIGATIONS INTO THE INCIDENT AND THEY HAVE DENIED THE CLAIM. THAT FURTHER INQUIRIES BE DIRECTED TO THE INSURANCE COMPANY. I HAD INQUIRED TO KNOW FROM CHRYSLER IF THEY HAD OTHER REPORTED INCIDENTS WITH POWER STEERING HOSES CAUSING FIRES TO THIS TYPE OF VEHICLE AND WHETHER THIS VEHICLE HAD ANY RECALLS. YET, NO ONE HAS ANSWERED THIS QUESTION. *TR
Jun 04, 2007
Fire: 1
AFTER DRIVING VEHICLE FOR APPROXIMITTLY 15 MIN I PARKED TO HAVE LUNCH. WHILE INSIDE SOMEONE RAN IN AND SAID A CAR WAS ON FIRE. MY CAR WAS TOWED TO DEALERSHIP AND AFTER INVESTIGATION OF FIRE I WAS TOLD BY THE MECHANIC HE HAD NEVER SEEN ANY THING LIKE THIS BEFORE, HE SAID THE GAS LINE LOCATED BEHIND ENGINE HAD EXPLODED FROM THE INSIDE OUT. WHICH IN TURN STARTED A FIRE.*AK
Jan 23, 2002
Fire: 1
STEERING,ENGINE AND ENGINE COOLING
2 complaints
1998 DODGE STRATUS CAUGHT ON FIRE IN THE ENGINE COMPARTMENT. DAUGHTER TURNED A CORNER WHEN THE POWER STEERING WENT OUT. SHE PULLED OVER AS THE ENGINE CAUGHT FIRE. IT WAS EXTINGUISHED BY THE FIRE DEPARTMENT.THE CAR WAS TOTALED. *JB
Nov 21, 2005
Fire: 1
WHILE THE VEHICLE WAS PARKED CONSUMER NOTICED FLUID LEAKING FROM UNDERNEATH THE VEHICLE. IT WAS TAKEN TO THE DEALER FOR INSPECTION, AND MECHANIC DETERMINED THAT HEAD GASKET NEEDED TO BE REPLACED. *AK THE CONSUMER STATED THAT THE TIE ROD FELL OFF. *TC
Dec 22, 2004
WHEELS
2 complaints
WHILE DRIVING 55 MPH, BOTH FRONTAL RIMS CRACKED. THIS CAUSED WHEEL TO CAVE IN. CONSUMER HAD VEHICLE TOWED TO THE DEALER FOR INSPECTION, AND MECHANIC TOLD CONSUMER THERE WAS NO DETERMINATION TO FIX THE RIM. *AK
Feb 03, 2004
THE RIGHT REAR WHEEL (RIM) HAS SMALL HOLES IN IT AND THE METAL SEEMS WEAK AND THE DEALER SAYS TOUGH LUCK. I BROUGHT THE PROBLEM TO THEIR ATTENTION ABOUT TWO TO THREE DAYS AFTER PURCHASE AND NO ONE COULD FIND THE PROBLEM. NOW MY WARRANTY HAS EXPIRED, AND THEY SAY IT HAS NEVER HAPPENED BEFORE. ARE THERE ANY PREVIOUS PROBLEMS WITH DODGE STRATUS RIMS 15INCH, 5 LUG, 5 SPOKE?*AK
Nov 08, 2001
SERVICE BRAKES, HYDRAULIC,ENGINE AND ENGINE COOLING
2 complaints
THE VEHICLE LOST OIL, AND THE BRAKE PEDAL TRAVELED TO THE FLOOR WHEN APPLIED. THE DEALER REPLACED THE BRAKE TUBE AND CLAMP. *JB
Apr 14, 2003
I TOOK MY CAR IN BECAUSE I NEEDED TO HAVE THE BRAKES REPAIRED AS A REGULAR ITEM OF REPAIR, SECONDARY TO WEAR AND TEAR. THIS WAS EARLY IN DECEMBER 2000. THE MECHANIC ALSO CHECKED OVER THE CAR AND REPORTED THAT AS WITH MANY 1998 DODGE STRATUS' I WILL NEED TO KEEP AN EYE ON THE CYLINDER HEAD GASKET. THE MECHANIC ALSO INFORMED ME THAT I SHOULD CHECK WITH THE DEALER AND SEE IF THIS ITEM HAS YET BEEN RECALLED. I THEN HAD NO PROBLEMS FOR THE NEXT FEW WEEKS WHEN I WAS TURNING AROUND A CORNER SLOWLY AND AN AWFUL NOISE OCCURRED. I THEN PARKED THE CAR AND WHEN I RETURNED I HAD A LARGE OIL LEAK ON THE GROUND. I SCHEDULED AN APPOINTMENT WITH MY TRUSTED MECHANIC AND THEY CHECKED IT OVER WHEN THEY NOTICED THAT THE HEAD GASKET NEEDED REPLACING, THE ENTIRE PULLEY SYSTEM WAS SEIZING UP AND NEEDED REPLACING AND MY MANIFOLD NEEDS TO BE REPLACED. THE COST OF THIS WAS $1,000 AND THAT WAS WITHOUT REPLACING THE MANIFOLD, AS I COULD NOT AFFORD IT AT THAT TIME. I HAVE CALLED THE DEALERSHIP AND THEY REPORTED THAT THEY WOULD HAVE TO SCHEDULE AN APPOINTMENT TO LOOK AT THE CAR, SUBMIT A CLAIM TO THE REGIONAL MANAGER OF DAIMLER CHRYSLER AND THEY HAVE BEEN KNOWN TO HELP OUT WITH APPROX. $200. OF THE REPAIRS. WELL SINCE I WAS IN THE PROCESS OF MOVING TO GA FROM CA AND HAD TO STAY ON SCHEDULE I WAS UNABLE TO STAY BACK FOR THE APPOINTMENT WHICH WASN'T UNTIL A WEEK LATER. UPONE MY REQUEST FOR THE NAME AND NUMBER OF THE REGIONAL MANAGER OF DAIMLER CHRYSLER, THEY SAID , I CANNOT GIVE THAT INFORMATION TO YOU. WE ARE THE ONLY ONES WITH THIS INFORMATION AND YOU MUST BRING TO CAR IN FOR US TO INSPECT. WHEN I ASKED THEM IF THIS INPECTION WOULD COST, THEY REPORTED, DEPENDING UPON THE TESTS NEEDED. I KNEW THAT FINANCIALLY, EVEN IF I WAS APPROVED FOR $200 ASSISTANCE I WAS BETTER OFF GETTING THIS FIXED BY A TRUSTED LESS EXPENSIVE MECHANIC AND FIGHT THE BATTLE LATER. CLEARLY A VEHICLE WITH 70,000 HWY MILES, WITH OIL CHANGES EVERY 3,500 MILES SHOULD NOT NEED A NEW MANIFOLD, A NEW PULLEY SYSTEM AND ALL NEW GASKETS
Feb 11, 2001
SEATS
2 complaints
I'VE LOST A SEAT PART TO MY CAR AND I'M HAVING TROUBLE GETTING IT FROM ANYONE. I'VE CONTACTED DODGE CUSTOMER SERVICE, HAD THE PART ON ORDER AND THEN THEY CANCELLED IT WITHOUT NOTIFYING ME OR TELL ME WHY. THE PART # IS RD161AZAA AND IS A PILLOW THAT CONNECTS TO AN INTERGRATED CHILD SEAT IN THE BACK. I'M NOW UNABLE TO USE THE ENTIRE BACK SEAT FOR FEAR THAT ONE OF MY CHILDREN WILL GET HURT. CAN YOU HELP? DT
Nov 27, 2002
WHILE DRIVING AND WITH NO WARNING DRIVERS SEAT FULLY RECLINED BACK, AND COULD HAVE CAUSED AN ACCIDENT. CAUSE UNKNOWN. DEALER NOTIFIED.*AK *YH
Jul 19, 2002
LATCHES/LOCKS/LINKAGES
2 complaints
ON SEVERAL OCCASIONS, CONSUMER HAD PROBLEMS WITH SHUTTING THE DRIVER SIDE AND PASSENGER SIDE DOOR, CONSUMER NOTICED THAT THE DOOR LATCHES WERE COMING UNDONE, DEALER REPLACED AT OWNERS EXPENSE. *TT
Apr 04, 2002
ON SEVERAL OCCASIONS, CONSUMER HAD PROBLEMS WITH SHUTTING THE DRIVER SIDE AND PASSENGER SIDE DOOR, CONSUMER NOTICED THAT THE DOOR LATCHES WERE COMING UNDONE, DEALER REPLACED AT OWNERS EXPENSE. *TT
Apr 04, 2002
ENGINE AND ENGINE COOLING,UNKNOWN OR OTHER
2 complaints
THEY WANT ME TO PAY $900 FOR A DEFECT THAT OCCURRED TO THE 1995 MODEL. NLM
Mar 26, 2002
Fire: 1
CHECK OIL LIGHT ALERTED ME TO A PROBLEM WHICH WAS CONFIRMED BY A LICENSED MECHANIC. THE PROBLEM IS A BLOWN HEAD GASKET. WHILE CAR WAS IN THE SHOP, MECHANICS SUGGESTED I LOOK FOR A RECALL. NONE AT THE PRESENT TIME. TALKED TO DODGE DEALER. WAS TOLD THAT SINCE I HAD OVER 75000 MILES AND A NON-DODGE MECHANIC WAS REPAIRING THE PROBLEM, THERE WAS NOTHING THEY COULD DO. IT HAS BECOME OBVIOUS THAT THIS IS A GROWING PROBLEM. THIS SHOULD BE ADDRESSED AS A RECALL. I CAUGHT IT EARLY. DODGE SHOULD STEP UP AND FIX THE PROBLEM, REGARDLESS OF THE NUMBER OF MILES ON THE VEHICLE. SOME POEPLE PROPERLY MAINTAIN THEIR VEHICLES. *AK
Jan 16, 2001
SERVICE BRAKES, HYDRAULIC,VEHICLE SPEED CONTROL
2 complaints
3 TIMES WITHIN 6 MONTHS ,TWICE WHILE AT A STOP AND ONCE WHILE DRIVING, BRAKES WILL START TO FADE AND VEHICLE WILL SUDDENLY SURGE/ACCELERATE , CONSUMER HAS TO SHIFT INTO PARK IN ORDER TO STOP VEHICLE.*AK
Nov 16, 2000
I WAS HEARING NOISED COMING FROM THE BRAKES AND TOOK CAR IN FOR INSPECTION, I WAS HANDED A LIST OF NOISES THAT WERE TO BE CONSIDERED NORMAL. I WENT IN A SECOND TIME WITH BLACK DUST ON OUTSIDE OF HUBCAPS AGAIN I WAS TOLD IT WAS NORMAL. THEN MY BRAKES FAILED WHILE BACKING OUT OF DRIVEWAY. DEALER REPLACE NUMEROUS PARTS OF FACTORY DEFECTIVE PARTS. ALSO I WAS STOPPED AT A TRAFFIC LIGHT AND VEHICLE ACELLERATED ON ITS OWN, I ALMOST HIT A PEDESTRIAN AND WENT INTO ONCOMING TRAFFIC. I HELD MY FOOT ON THE BRAKE TO TRY TO KEEP THE VEHICLE FROM MOVING. THE VEHICLE WAS JUMPING FROM SIDE TO SIDE AND SMOKING WHILE THE ENGINE WAS RACING AT MAX THROTTLE.
Sep 18, 1999
EQUIPMENT
2 complaints
WHILE DRIVING A/C STOPPED BLOWING. CONSUMER SHUT CAR OFF AND SMOKE WAS COMING OUT FROM UNDER THE HOOD, TOOK TO DEALER, AND THEY SAID THAT CLUTCH FOR THE A/C COMPRESSER WAS HANGING UP AND BURNED UP THE COMPRESSER.*AK
Aug 21, 2000
ON SATURDAY JUNE 17, 2000 WHILE TRAVELING IN LEWISBURG TN , IT STARTED RAINING HEAVILY. HAD RAN THE AIR CONDITIONER EARLIER IN THE DAY BUT AFTER SOME SHOWERS IT HAD COOLED THINGS DOWN AND JUST HAD ON THE AIR VENTS. AFTER ENCOUNTERING HEAVY RAIN TURNED THE DEFROSTER ON TO CLEAR FOGGY WINDOWS AND HEARD A HOWLING GRINDING NOISE FROM UNDER THE HOOD. IMMEDIATELY PULLED OFF THE ROAD AFTER TURNING THE DEFROSTER OFF. TRIED IT AGAIN AND SAME NOISE AND ALSO TRIED TO TURN ON AIR CONDITIONER WITH SAME RESULTS AND CAR CHOKED OUT AND QUIT. SO I JUST TURNED OFF THE COMPRESSOR AND USED VENT ONLY TO TRY TO GET HOME. I ACCESSED YOUR WEBSIT FOR INFO REGARDING STRATUS. I F OUND INFO ON TECH SERV BULLETINS ABOUT COMPRESSOR FAILURE AT 90+ TEMPS WE HAVE HAD 90+ MORE THAN NOT SINCE MAY. CONTACTED THE DEALER MONDAY MORN ABOUT PROBLEM TALKED TO GEN MGR. MR. STEPHENS HE TOLD ME TO BRING INFO AND CAR IN WED FOR FREE INSPECTION OF PROBLEM. I TOOK THE CAR IN AND TRIED TO TALK TO HIM AND SERV DEPT ABOUT COMPRESSOR FAILURE PROBLEMS. THEY SAID THEY WOULD CHECK OUT COMPRESSOR AND CALL ME. THEY CONFIRMED COMPRESSOR LOCKED UP ON CAR AND OFFERED TO FIX THE CAR FOR 700.00 INSTEAD OF REG PRICE OF 940.00 SINCE THE CAR WAS OUT OF WARRANTY AT 36,000 MILES THATS THE BEST THEY WOULD DO. I ARGUED ACCORDING TO INFO I HAD F OUND AND BROUGHT TO THERE ATTENTION I THOUGHT THE PROBLEM WAS A DEFECTED COMPRESSOR AND THEY SHOUD FIX AT NO COST. THEY SAID NO. I WENT AND PICKED UP CAR AND F OUND CERTIFIED A/C TECH CAR REPAIR PLACE TO DO THE WORK FOR MUCH LESS. WHEN CHECKING AROUND FOR ESTIMATES ONE AUTO REPAIR SHOP TOLD ME I WAS THE 5 INQUIRY ABOUT FAILED A/C COMPRESSOR ON 98 STRATUS. I FEEL THAT THIS IS A MFG DEFECT AND POSES A SAFETY PROBLEM WHEN IT LOCKS UP GOING DOWN STREET OR HWY BECAUSE IT CHOKES OUT THE ENGINE AND COULD CAUSE AN ACCIDENT AND INJURY ESP CONSIDERING THE MILEAGE ON CAR I HAVE F OLLOWED ALL REASONABLE MAINT GUILDLINES AND IN MY OPINON THIS COMPRESSOR SHOULD HAVE LASTED LONGE
Jun 22, 2000
STRUCTURE
2 complaints
REAR AND FRONT HATCH FAILED.
Mar 12, 1999
TRUNK IS SO HIGH THAT IT IS IMPOSSIBLE ANYTHING DIRECTLY BEHIND THE VEHICLE.
Oct 26, 1998
STRUCTURE,ENGINE
1 complaint
FIRST HORN WAS BLOWING OUT OF CONTROL, THAN THE ENGINE WE GOT IT FIXED, OR SO WE THOUGHT ,THAN GOT THE STARTER FIX DROVE IT 2 WEEKS AND NOW IT TURNS OVER BUT DOES NOTHING SO IT'S SITTING IN MY YARD NOT WORKING AND AM SICK OF IT SO FAR I HAVE PAID OUT OVER A GRAND AND THIS CAR DON'T WORK JUST WHY,OH GOD JUST WHY.I HAVE PAID SOME OF EVERYTHING YOU THINK OF ONE THAT CAR I HAVE HAD IT TOWARDS SO MUCH STATE FARM WANTED TO CANCEL MY INSURANCE, OKAY LET'S BEGIN.STARTER REPLACED,EG ROAD VALVE SENSER,VALLEY + PIPE, IGNITION COIL,IGNITION RELAY,TEMPERATURE SENSER,IGNITION WIRE, ROTOR, INJECTOR, BRUSH, BEARING BALL, DECEMBER FRAME NOT TO MENTION THE LABOR MY GOD. AND NOW IT SITS IN MY YARD AM TIRED REALLY.
Jan 17, 2017
SERVICE BRAKES
1 complaint
THE ABS AND THE BRAKING SYSTEM QUIT WORKING I GOT ON THE FREEWAY AND I HAD BREAKS BY THE TIME I GOT THREE OFF RAMPS LATER TO GET OFF THE FREEWAY I HAD NO BRAKES THEY DIDN'T WORK IN THE PEDAL WENT ALL THE WAY TO THE FLOOR CAUSING AND ACCIDENT
Apr 27, 2016
Crash: 1
SUSPENSION,ELECTRICAL SYSTEM,ENGINE
1 complaint
HAVING ISSUES WITH DASH AND HEADLIGHT DIMMING,ALSO RADIO GOES OFF AND LOOSES MEMORY,DOOR LOCKS WON'T WORK WHEN RADIO GOES OFF. BURNT OUT DEFOGGER RELAY AND POWER AMP FUSE WITH NO POWER AMP, ALSO HAD TO REPLACE HORN RELAY YET TAKING ALL THOSE RELAYS OUT AND PROBLEM STILL HAPPENS. ALREADY CHECKED LIGHTER ASSEMBLY, THAT WAS POPPING AMP FUSE. FIXED THAT STILL HAPPENING. ALSO GOES THROUGH 1 QUART OF OIL A MONTH BUT NO LEAKS UNDER THE CAR WHEN MOVED. ?????? HELP!!!!!! THE OIL PROBLEM SHOULD FALL UNDER HAZARDOUS METERIALS ACT IF ALL THESE CARS ARE DUMPING USED OIL ALL OVER THIS COUNTRY.
Nov 01, 2015
SUSPENSION,ELECTRICAL SYSTEM,FUEL/PROPULSION SYSTEM
1 complaint
TL* THE CONTACT OWNS A 1998 DODGE STRATUS. WHILE THE VEHICLE WAS AT THE DEALER FOR ROUTINE MAINTENACE, IT WAS DISCOVERED THAT THE FRONT BALL JOINT AND CONTROL ARM NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. ON TWO SEPARATE OCCASIONS, THE VEHICLE FAILED TO START. THE VEHICLE WAS TAKEN TO THE DEALER FOR DIAGNOSTIC TESTING. THE DEALER DETERMINED BOTH TIMES THAT THE FUEL PUMP NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED BOTH TIMES. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. SEVERAL YEARS LATER, THE CONTACT WAS UNABLE TO REMOVE THE KEY FROM THE IGNITION SWITCH. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBERS: 04V021000 (POWER TRAIN) AND 98V183000 (POWER TRAIN). THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURES. THE FAILURE MILEAGE WAS 5,000.
Aug 26, 2015
POWER TRAIN,ELECTRICAL SYSTEM
1 complaint
TL* THE CONTACT OWNS A 1998 DODGE STRATUS. THE CONTACT STATED THAT THE GEAR SHIFTED FROM PARK WITHOUT THE KEY IN THE IGNITION. THE CONTACT ALSO STATED THAT THE KEY BECAME STUCK IN THE IGNITION. THE FAILURE OCCURRED ON MULTIPLE OCCASIONS. THE CONTACT REFERENCED NHTSA CAMPAIGN ID NUMBER: 04V02100 (POWER TRAIN), HOWEVER, THE VEHICLE WAS NOT AFFECTED AT THE TIME AND NO REPAIRS WERE DONE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 50,000.
Jun 18, 2014
TIRES
1 complaint
1998 DODGE STRATUS RIGHT FRONT TIRE BLEW OUT WHILE PULLING INTO A TOLL BOOTH LANE. *KB OHIO TRAFFIC CRASH REPORT # 10-0765-90. *JB
Sep 16, 2009
Crash: 1
EXTERIOR LIGHTING
1 complaint
THE HEAD LIGHT LENS COVER IS VERY CLOUDED FROM A DEFECT IN THE PLASTIC THE WRONG TYPE OF PLASTIC WAS USED FOR THE HEADLIGHT THAT DEALS WITH THE ELEMENTS AND THE DOES THAT WHILE DRIVING DOWN THE ROAD. THIS INTERNS REDUCES THE LIGHTING FROM THE HEAD LIGHTS SO BAD THAT IT IS HARD TO SEE AT NIGHT AND IM 23 AND HAVE 20\20 VISION. I CAN DRIVE WITH MY BRIGHTS ON AND THE LIGHT IS STILL WEAKER THAN MOST OF THE CARS DRIVING DOWN THE ROAD. I HAVE NOTICED THAT OTHER 1998 DODGE STRATUS CARS HAVE HAD THE SAME PROBLEM UNLESS NOT DRIVEN MUCH AND GARAGED. SPEAKING TO A QUALITY CONTROL MANAGER AT GRIMM BROTHERS PLASTICS IN WAPELLO IOWA HE TOLD ME THAT THE WRONG PLASTIC WAS USED FOR THE HEADLIGHT. I HAVE RECENTLY ALMOST BEEN IN AN ACCIDENT WITH MY 2 YEAR OLD DAUGHTER AND NOW DO NOT DRIVE THE CAR AT NIGHT. AND ITS MY ONLY CAR. *NM
Dec 10, 2006
STEERING,AIR BAGS
1 complaint
DT: THE CONTACT COMPLAINED ABOUT STEERING PROBLEMS. THE STEERING WHEEL FELT AS THOUGH IT WAS BINDING. THE POWER STEERING FLUID WAS KEPT AT CORRECT LEVELS. THE VEHICLE EXPERIENCED STEERING DIFFICULTIES FOR THE PAST YEAR. THE VEHICLE WAS INVOLVED IN A CRASH AND THE AIR BAGS DID NOT DEPLOY. THE VEHICLE RAN INTO A HILL AND NEITHER AIR BAG DEPLOYED. THE SPEED WAS AROUND 55 MPH. THE MANUFACTURER HAS NOT BEEN CONTACTED ABOUT THE STEERING OR THE AIR BAGS. A POLICE REPORT WAS TAKEN FROM THE CRASH.*AK UPDATED 1/5/2006 - THE CONSUMER WAS INJURED AND HAD TO BE TAKEN BY AMBULANCE TO THE HOSPITAL. *NM
Nov 08, 2005
Crash: 1
Injuries: 1
STEERING,SERVICE BRAKES, HYDRAULIC
1 complaint
BRAKES, OUTER TIE ROD, BRAKE CALIPERS, ENGINE OIL INNER SEAL. BRAKE PADS, SINCE I HAVE OWNED THIS CAR I HAVE REPLACED THE BRAKE PADS 20 TIMES EVERY 3 MONTHS AND THE BRAKE CALIBER ON THE RIGHT REAR THIS WILL MAKE THE 9TH TIME I AM RUNNING OUT OF MONEY ON THIS CAR THE FRONT BRAKES AND HUBS HAVE BEEN REPLACED SEVERAL TIMES HAVE ALL MY RECEIPTS AND CAN PROVE THE WORK THAT HAS BEEN DONE ON MY CAR COST OF OIL LEAK REPAIR WAS OVER $800.00 DOLLARS AND GUESS WHAT I WILL HAVE THE CAR PAID FOR THIS MONTH AND I AM STILL WORKING ON THE WHEELS AND BRAKES I NEED SOME HELP WITH THIS CAR AND THE DEALERSHIP I PURCHASED THE CAR FROM WILL NOT RESPOND TO MY QUESTIONS ABOUT THE BRAKES, AND THE ENGINE PROBLEMS I AM HAVING. *AK
Oct 02, 2004
PARKING BRAKE
1 complaint
THREE MONTHS AFTER INSTALLATION OF A NEW EMERGENCY BRAKE CABLE, THE CABLE BROKE AND VEHICLE HAD A RUNAWAY. *LA TWO CABLES ON THE SAME SIDE BROKE IN THREE MONTHS. TWO DEALERS SUGGESTED THAT THE PROBLEM WILL CONTINUE TO RECUR. (DODGE DUALLY) *SC
Feb 12, 2004
Crash: 1
STEERING,SUSPENSION
1 complaint
SINCE JULY 2003, I HAVE HAD TO REPLACE LEFT AND RIGHT TIE RODS AND RIGHT WHEEL BEARING. 7/2003-LEFT TIE ROD, 8/2003 RIGHT WHEEL BEARING, 1/2004 RIGHT TIE ROD. *JB
Feb 01, 2004
ENGINE AND ENGINE COOLING,LATCHES/LOCKS/LINKAGES
1 complaint
1998 DODGE STRATUS 2.4L ENGINE AUTOMATIC 1. THE ENGINE IS SEVERLY LEAKING OIL. TWO MECHANICS HAVE LOOKED AT IT AND BOTH SAID IT NEEDS A NEW HEAD GASKET. THIS CAR ONLY HAS 76,000 MILES ON IT. UPON RESEARCH, THIS IS A RAMPANT PROBLEM. I HAVE SEEN HUNDREDS OF COMPLAINTS. THEY HAVE CHANGED THE GASKET TYPE TO FIX THIS PROBLEM. THIS SHOULD BE A RECALL ITEM! 2. TRUNK LATCH SEEMS TO HAVE A STICKING PROBLEM. THIS TOO SEEMS TO BE A VERY COMMON PROBLEM. *LA
Oct 05, 2003
ENGINE AND ENGINE COOLING,EQUIPMENT
1 complaint
I'VE STARTED EXPERIENCING BOTH HEAD GASKET LEAKS AS WELL AS AIR CONDITION ISSUES. I HAVE PAID OUT OVER $2,500 COMBINED OVER THE PAST 18 MONTHS. NOW, I READ THAT THIS IS SOMETHING THAT EVERYONE THAT HAS A 1998 DODGE STRATUS.*AK
Jul 17, 2003
ENGINE AND ENGINE COOLING,FUEL SYSTEM, GASOLINE,LATCHES/LOCKS/LINKAGES
1 complaint
MY DODGE STRATUS/98 HAS RECENTLY BEGAN GIVING ME A LOAD OF PROBLEMS.IT ALL BEGAN SUMMER 2001 WITH THE DRIVERS SIDE DOOR NOT BEING ABLE TOO CLOSE.I DID NOT THINK ANYTHING WAS WRONG UNTILL I ATTEMPTED TO CONTINUOUSLY CLOSE MY DOOR AND IT WOULD NOT SHUT.SO I LOOKED CAREFULLY AND THE LATCH THAT LOCKS THE DOOR IN PLACE WAS COMMING UNDONE.I THAN TRIED TO MAKE THE DOOR SHUT BUT THE PROBLEM WAS GREATER THAN THAT.THE SCREW WAS GONE AND THE SECOND WAS ALMOST OUT OF TACT.THE LABOR AND SCREW REPLACEMENT ALONG WITH THE TOWE COST ME AROUND $60.00.THAN LUCK WOULD HAVE IT THE SAME INCIDENT OCCURED AGAIN ON THE LEFT-HAND FRONT PASSENGER SIDE WITH LABOR AND PARTS COSTING $30.00.THE PROBLEM WITH MY ENGINE BEGAN IN NOVEMBER, I HAD NOTICED THAT MY CAR OIL AND ENGINE WARNING HAD APPEARED SO I TOOK MY CAR TO A MECHANIC HAD OIL-FILTERS,AIR-CONDITION FLUID,WATER,& ENGINE ALL CHECKED AND REPAIRED.THE MECHANIC TOLD ME ALL I NEEDED AND $360.00 WAS WELL INVESTED.I THOUGHT ALL WAS FINE BUT THE SERVICE SIGNAL FOR OIL AND SOMETIMES ENGINE WERE CONSTANTLY APPEARING. I TOOK MY CAR BACK AND THE MECHANIC TOLD ME THAT I NEEDED MORE OIL AND WHEN DID I LAST HAVE MY CAR CHECKED,I ADVISED HIM THAT IT WAS NOT LONG AGO HE THAN EMPHASIZED THAT I WAS LUCKY MY CAR HAD NOT LOCKED.THE NEXT WEEK THE SAME THING BUT ANOTHER MECHANIC.HE TOLD ME MY OIL WAS LEAKING HE COULD NOT DETERMINE FROM WHERE SO HE RECOMMENDED I CHANGE MY OIL-FILTERS,OIL BRAND AND PUT CAR ON MACHINE DIALIYSIS.HE DID ALL THIS TOTALING $73.00.YET A WEEK LATER I'M HAVING TO PLACE UP TO THREE QUARTS OF OIL EVERY WEEK.I CONTACTED A LOCAL DODGE DEALER HERE IN EASTMAN GA 31023 AND HE TOLD ME OF DAIMLER LUCK WOULD HAVE IT YOU ALL HAD JUST SENT ME NOTIFICATION OF BRAKE CHANGE. I MADE THE COMPLAINT AND NO ONE CONTACTED ME SO NOW TODAY I HAD A BAD ACCIDENT MY CAR COMPLETLY STOPPED LEAVING ME STRANDED AND WHEN MY CAR STOPPED IT JERKED ME LEAVING ME STUNNED BUT CONCIOUS AND MY CAR IS NOW OUT OF SERVICE. *AK
Mar 30, 2002
Injuries: 1
ENGINE AND ENGINE COOLING,VISIBILITY,SEAT BELTS
1 complaint
I HAVE HAD NUMEROUS PROBLEMS WITH THIS VEHICLE, OTHER THAN THOSE LISTED, PLUS THERE IS MUCH MORE INFORMATION TO SUPPORT THE PROBLEMS I HAVE LISTED. I HAVE EXPERIENCED A HEATER CORE FAILURE, BRAKES REPLACED ALREADY TWICE ON THE VEHICLE WITH LESS THAN 40,000 MILES ON THE CAR. I HAVE HAD A DEFECTIVE SEAT BELT (PASSENGER), THE TIMING CHAIN IS A MAJOR ENGINE REPAIR THAT I JUST HAD DOWN. NOW I AM STILL DEALING WITH THE RESIDULE PRODBLEM WITH MY HEATING/DEFROST SINCE K & M REPLACED MY WATER PUMP ON 10/17/01. OVERALL I CONSIDER THIS CAR TO BE A REAL PIECE OF CRAP AND I ABSOLUTELY WOULD NEVER BUY ANOTHER STRATUS AND IN FACT, I WILL NEVER BUY ANOTHER CHRYSLER VEHICLE EVER. I FEEL I HAVE STUNG WITH A LEMON AND BASICALLY I NO LEGAL RECOURSE WHICH IS VERY UNFAIR TO ME, THE CONSUMER. I AM STILL PAYING ON THIS PIECE OF CRAP. IF NOTHING ELSE, I HOPE TO WARN ANYBODY ELSE, PLEASE DO YOUR HOMEWORK AHEAD OF TIME AND DON'T BUY A DODGE STRATUS. ANY ASSISTANCE NHTSA MIGHT OFFER WOULD BE GREATLY APPRECIATED. I CAN PROVIDE ANY DOCUMENTATION AND DETAIL THAT YOU REQUIRE. THANK YOU.
Nov 14, 2001
SUSPENSION,ENGINE AND ENGINE COOLING,POWER TRAIN
1 complaint
NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK
Dec 26, 2000
ENGINE AND ENGINE COOLING,POWER TRAIN
1 complaint
THIS CAR HAS BEEN A MAJOR PROBLEM. HEAD GASKET FAILED AT APPROX 11,000 ON MY WAY TO AIRPORT TO PICK UP FAMILY ON APRIL 10, 1999. COULDN'T GET IT IN FOR SERVICE UNTIL APRIL 14, 1999. TRANSMISSION CLUTCH STARTED CATCHING OR SCRAPING ON SOMETHING SHORTLY AFTER HEAD GASKET WAS REPLACED, I WAS TOLD WHEN WORK WAS COMPLETED (REPLACED CABLES ON 11/18/1999) THAT PROBLEM WAS MANUFACTURER DEFECT MILEAGE WAS 18,373. WAS AGAIN EXPERIENCING SAME PROBLEM WITH CLUTCH ON 2/29/2000. UPON SPEAKING WITH SERVICE TEAM, WAS TOLD THERE WAS A BAD BEARING IN THE TRANSMISSION AND THEY WOULD BE REPLACING BOTH THE CABLES AND TRANSMISSION PARTS; I ALSO ASKED FOR THEM TO CHECK THE ENGINE LIGHT , BECAUSE IT WAS COMING ON AND HAD A STRONG SMELL OF GASOLINE; VACCUM SYSTEM WAS REPLACED. ON 3/24/2000 INTERNAL PARTS OF TRANSMISSION WERE REPLACED AT 22,349 MI. ON 06/05/2000 ENGINE STALLED AND WAS DIFFICULT TO RESTART, ENGINE WAS RUNNING REALLY ROUGH, REPLACED MAPPING COMPUTER @25,008 MI. CAME HOME FROM WORK ON 8/23/2000 STRONG ODOR OF GASOLINE. OPENED HOOD AND WATCHED GAS LEAKING ALL OVER EXHAUST MANIFOLD. HAD IT TOWED TO DEALERSHIP ON 8/24/2000 W/ 29,539 MI. REPLACED CRACKED FUEL INJECTORS AND LEAKING HOSES. THE CAR IS NOW IN AGAIN BECAUSE OF YET THE SAME TRANSMISSION/CLUTCH PROBLEM PREVIOUSLY COMPLAINED ABOUT. THINK . . . I'M DRIVING DOWN I 95 WITH MY FAMILY IN MY CAR. TRANSMISSION FAILS, BIG TRUCK RUNS THE CAR OVER . . . DOES CHRYSLER WANT THAT HEADACHE?
Nov 07, 2000
CHILD SEAT
1 complaint
WE HAVE CONCTACED SEVERAL CAR SEAT MANUFACTURERS (FISHER PRICE AND EVEN-FLO) AND THEY DO NOT RECOMMEND USING CONVERTIBLE CAR SEATS IN THE REAR POSITION WITH AUTOMATIC EMERGENCY LOCKING DEVICE SEAT BELTS WHICH IS IN MY DODGE STRATUS. WE CONTACTED CHRYSLER AND THEY TOLD US THERE WAS NOTHING THEY COULD DO TO SOLVE THE PROBLEM. I THINK IT IS VERY IMPORTANT TO INFORM THE PUBLIC THAT TO MY KNOWLEDGE THERE IS NOT A SAFE CHILD SEAT MADE THAT WILL WORK IN THE REAR POSITION IN A CAR WITH A AUTOMATIC EMERGENCY LOCKING DEVICE. THIS I ASSUME INCLUDES ALL OR MOST CHRYSLER VEHICLES. WE INFORMED THEM THAT THERE ARE THOUSANDS IF NOT MILLIONS OF PARENTS TRAVELING AROUND THE DAILY WITH CARS THAT ARE NOT CAPABLE OF BEING USED WITH REAR FACING CHILD SEATS. THEY NEED TO ADDRESS THIS ISSUE. IT IS DISAPPOINTING THAT A CAR MAKER COULD EVEN PRODUCE A PRODUCT WITH SURE DISREGARD FOR CHILD SAFETY.
Apr 07, 2000
ENGINE AND ENGINE COOLING,VISIBILITY,UNKNOWN OR OTHER
1 complaint
I NOTICED MY CAR OIL LIGHT CAME ON - SO I CHECKED THE OIL AND MUCH TO MY AMAZEMENT I SHOWED NO OIL LEVEL ON THE DIP-STICK SO I ADDED OIL UNTIL IT SHOWED ON THE DIP-STICK WHICH ENDED UP BEING 2 QTS LOW. SINCE JANUARY I HAVE ADDED AT LEAST 3 QTS A DAY, COSTING ME A NUMEROUS AMOUNT OF MONEY. ALSO MY WINDSHIELD HAS BEEN CRACKING SINCE FEB, 99 THE CRACK HAS ALMOST REACHED THE DRIVERS SIDE. *AK
Mar 08, 2000
STEERING,UNKNOWN OR OTHER
1 complaint
WHILE DRIVING INTO A PARKING LOT THE RUBBER BOOT IS TOO SMALL THAT IT WON'T SLIDE OVER THE COUPLING MECHANISM TO KEEP SOMETHING FROM GETTING INTO IT. THE FACTORY ISSUED FLOOR MAT GOT CAUGHT IN THE TURN COUPLING, AND DRIVER COULDN'T TURN THE WHEEL. AVOIDED A NEAR MISS. CONTACTED DEALER. *AK
Feb 10, 2000
STEERING,POWER TRAIN
1 complaint
FLOOR SHIFT INDICATOR DOES NOT SHIFT PROPERLY. INDICATOR IS LOCATED ON DASHBOARD & NOT SHOWING WHAT GEAR VEHICLE IS LOCATED IN. ALSO, STEERING WHEEL TILTS WHERE IT OBSTRUCTS THE VIEW OF THE INDICATOR. *AK
Jan 20, 1999
SERVICE BRAKES, HYDRAULIC,EXTERIOR LIGHTING,VISIBILITY
1 complaint
WHEN DRIVING AT ANY SPEED AND APPLYING THE BRAKES THERE IS A VERY LOUD NOISE COMING FROM THE BRAKES. ALSO, THE CONSUMER IS HAVING PROBLEMS WITH THE PASSENGER'S WINDOW, WHERE THERE IS AIR COMING THROUGH THE WINDOW. IN ADDITION, THE TURN SIGNAL LIGHTS WORK INTERMITTENTLY. THE COSNUMER CAN'T DETERMINE THE PROBLEM. *AK
Nov 18, 1998
4.3/5.0
78 reviews

Frequently Asked Questions

How many problems does the 1998 DODGE Stratus have?

The 1998 DODGE Stratus currently has 292 owner-reported complaints according to NHTSA database. These complaints are organized by component to help identify common issues.

What are the most common problems with 1998 DODGE Stratus?

The most common problems reported for the 1998 DODGE Stratus are organized by component above. Each component section shows owner-reported issues, crash reports, and fire incidents to help identify patterns and problem areas.

Where does this 1998 DODGE Stratus problem data come from?

All problem and complaint data for the 1998 DODGE Stratus comes directly from the National Highway Traffic Safety Administration (NHTSA) database. These are real complaints submitted by actual vehicle owners.

Other Years - DODGE Stratus

Other DODGE Models

Similar Brands

← Back